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Fire Dynamics Simulation of 2011 Baltimore County LODD- 30 Dowling Circle

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Operations at 30 Dowling Circle 01.19.2011 Box 11-09

 On Wednesday, January 19, 2011, a fire occurred in an apartment building located in the Hillendale section of Baltimore County, Maryland. This fire resulted in the line of duty death (LODD) of volunteer firefighter Mark G. Falkenhan, who was operating as the acting lieutenant on Squad 303 . Upon their arrival, FF Falkenhan and a second firefighter from Squad 303 deployed to the upper floors of the apartment building to conduct search and rescue operations. Other fire department units were already involved with both firefighting operations and effecting rescues of trapped civilians.

During these operations, FF Falkenhan and his partner became trapped in a third floor apartment by rapidly spreading fire and smoke conditions. The second firefighter was able to self-egress the building by diving headfirst down a ladder on the front (address side) of the building. FF Falkenhan declared a “MAYDAY” and implemented “MAYDAY” procedures, but was unable to escape or be rescued.

FF Falkenhan was located and removed via a balcony on the third floor in the rear of the building. Resuscitative efforts began immediately upon removal from the balcony, and continued en route to the hospital. FF Falkenhan succumbed to his injuries and was pronounced deceased at the hospital.

Mark Gray Falkenhan had dedicated his life to serving others. He perished in the line of duty on January 19, 2011 while performing search and rescue operations at a multi-alarm apartment fire in Hillendale, Baltimore County (Maryland). He was 43 years old.

 

Firefighter Mark Falkenhan

30 Dowling Circle

 

The Baltimore County (MD) Fire Department published the Line of Duty Death Investgation Report of the 30 Dowling Circle Fire recently.

The report was written by a Line of Duty Death Investigation Team comprised of departmental members, including representatives of the local firefighters’ union and the Baltimore County Volunteer Firemen’s Association.

An overview and executive narrative of the final report (PDF) on the apartment fire where Volunteer Firefighter Mark Falkenhan sustained fatal injuries was posed on CommandSafety.com HERE.

FF Mark Falkenhan

 On Wednesday, January 19, 2011, a fire occurred in an apartment building located in the Hillendale section of Baltimore County, Maryland. This fire resulted in the line of duty death (LODD) of volunteer firefighter Mark G. Falkenhan, who was operating as the acting lieutenant on Squad 303 (for purposes of this report, Mark will be referred to as FF Falkenhan).

Upon their arrival, FF Falkenhan and a second firefighter (FF # 2) from Squad 303 deployed to the upper floors of the apartment building to conduct search and rescue operations. Other fire department units were already involved with both firefighting operations and effecting rescues of trapped civilians.

During these operations, FF Falkenhan and FF # 2 became trapped in a third floor apartment by rapidly spreading fire and smoke conditions. FF # 2 was able to self-egress the building by diving headfirst down a ladder on the front (address side) of the building. FF Falkenhan declared a “MAYDAY” and implemented “MAYDAY” procedures, but was unable to escape or be rescued.

FF Falkenhan was located and removed via a balcony on the third floor in the rear of the building. Resuscitative efforts began immediately upon removal from the balcony, and continued en route to the hospital. FF Falkenhan succumbed to his injuries and was pronounced deceased at the hospital.

The investigating team examined any and all data available, including independent analysis of the self contained breathing apparatus (SCBA), turnout gear and autopsy report. The Bureau of Alcohol, Tobacco, Firearms and Explosives (ATF) produced a fire model to assist with evaluating fire behavior. Multiple site inspections were conducted. Extensive interviews were conducted by the team which also attended those conducted by investigators from the National Institute for Occupational Safety and Health (NIOSH). Photographic and audio transcripts were also thoroughly analyzed. A comprehensive timeline of events was developed. All information used to make decisions regarding recommendations was corroborated by at least two sources.

  • In fairness to those units involved in this incident, the investigating team had the advantage of examining this incident over the period of several months. Furthermore, given the size and nature of the event, and the fact that arriving crews were met with serious fire conditions and several residents trapped and in immediate danger, all personnel should be commended for their efforts for performing several rescues which prevented an even greater tragedy.
  • The team did not identify a particular primary reason for FF Falkenhan’s death.
  • What were identified were many secondary issues involving but not limited to crew integrity, incident command, strategy and tactics, and communications.
  • These issues are identified and discussed, and recommendations are made in appropriate sections of the report, as well as in a consolidated format in the Report Appendix.

Some of the issues identified in this report may require some type of change to current practices, policies, procedures or equipment. Most, however, do not. Specifically, the analysis and recommendations regarding Incident Command and Strategy and Tactics show that if current policies and procedures are adhered to, the opportunity for catastrophic problems may be reduced.

  • Mark Falkenhan was a well-respected and experienced firefighter.
  • He died performing his duties during a very complex incident with severe fire conditions and unique fire behavior coupled with the immediate need to perform multiple rescues of victims in imminent danger.
  • It would be easy if one particular failure of the system could be identified as the cause of this tragedy.
  • We could fix it and move on. Unfortunately it is not that simple.
  • No incident is “routine”. Mark’s death and this report reinforce that fact.

On Wednesday, January 19, 2011 at 1816 hours, a call was received at the Baltimore County 911 Center from a female occupant at 30 Dowling Circle in the Hillendale section of Baltimore County. The caller stated that her stove was on fire and the fire was spreading to the surrounding cabinets. Fire box 11-09 was dispatched by Baltimore County Fire Dispatch (Dispatch) at 1818 hours consisting of four engine companies, two truck companies, a floodlight unit, and a battalion chief. All units responded on Talkgroup 1-2.

The location, approximately one mile from the first dispatched engine company, is a three story garden-type apartment complex, with brick construction and a composite shingle, truss supported roof. The fire building contained a total of six apartments divided by a common enclosed stairway in the center with one apartment on the left and one to the right of the stairs.

 

Fire Dynamics Simulation of 2011 Baltimore County LODD- 30 Dowling

Fire Dynamics Analysis and Insights

 

INTRODUCTION:

Assistance from the Bureau of Alcohol, Tobacco, Firearms and Explosives (ATF) Fire Research Laboratory (FRL) was requested for a fire at 30 Dowling Circle by the Baltimore County Fire Investigation Division (FID) through the ATF Baltimore Field Division on the night of January 19, 2011.

ATF Fire Protection Engineers were asked to utilize engineering analysis methods, including computer fire modeling, to assist with determining the route of fire spread and the events that led to the firefighter MAYDAY and subsequent Line of Duty Death.

Download the REPORT HERE

BACKGROUND:

Working closely with the Post Incident Analysis Team, the ATF Fire Research Laboratory created a computer simulation of the garden apartment building using Fire Dynamics Simulator (FDS). FDS is a computational fluid dynamics (CFD) modeling program developed by the National Institute of Standards and Technology (NIST).

FDS utilizes mathematical calculations to predict the flow of heat, smoke and other products of fire. Smokeview, a post-processer computer program also produced by NIST, was then used to visualize the mathematical output from FDS. The most current available versions of both programs were used: FDS 5.5.3 and Smokeview 5.6. Below are photographs of the front and rear of the fire building next to an image of the same building constructed in FDS.

Figure 01. 30 Dowling Street

 

Figure 2. FDS representation of the front of 30 Dowling Circle showing the terrace (T), second (A) and third (B) levels.

 

The garden apartment building at 30 Dowling Circle was attached to two similar garden apartment buildings, one on each side. The fire damage was isolated to 30 Dowling Circle, so the exposure buildings were not included in the computer fire model. The entire six unit garden apartment building was modeled in FDS, including the patio and balconies on the rear of the building. FDS works by dividing a space into cubical “grid cells” for calculation purposes. FDS then computes various CFD calculations for each grid cell to predict the movement of mass, energy, momentum and species throughout a three-dimensional space.

The Dowling Circle model consisted of 2,560,000 total grid cells that were each 3.9 inch (10 cm) cubes. The model was used to simulate a total elapsed real time of 27.5 minutes, beginning before the 911 call and ending just after flashover of the third floor and the firefighter MAYDAY.

The model was synchronized in real time with the fireground audio throughout the duration of the fire.

Fiqure 03 and 04

 

FDS has been validated to predict the movement of heat and smoke throughout a compartment, however the accuracy of fire modeling depends on it being used appropriately by a trained user that is aware of its limitations. Due to lack of knowledge about the exact material properties for the various furnishings and other available fuels, a user-specified fire progression was used for this application.

For flame and fire gas movement after consumption of the original burning fuel packages, the fire model calculated smoke and ventilation flow paths through the building and was used to gain a better understanding of the rapid fire growth leading to flashover of the stairwell and third floor.

  • In addition, FDS was utilized to illustrate the complex route of fire spread through the building as verified by witness statements, firefighter interviews, photographs and burn patterns.
  • Input data for the computer model included heat release rate data and video from previous testing conducted by the ATF FRL and NIST.
  • Ambient weather data was also input into the model, including temperature, as well as wind direction and magnitude at the time of the fire. In addition, several alternative compartmentation scenarios were modeled to explore the possible effects of closed stairway apartment entrance doors on the spread of smoke and flames in the stairwell.
  • The statements of each firefighter were reviewed and their individual actions (breaking windows, opening doors, etc.) and observations (fire size, smoke conditions, etc.) were recorded on floor diagrams.

The actions and observations of the firefighters were then associated with specific times in the fireground audio to generate an overall event timeline. All events in the model are based on this master timeline of events. In addition, all photographs were time stamped and synchronized with the model. The Post Incident Analysis Team was consulted throughout the development of the event timeline and the computer fire model to ensure accuracy.

MODELING ANALYSIS:

1. Analysis of Fire Development in the Terrace Level

The fire originated on the stovetop of an occupied apartment on the right (south) side of the terrace level (apartment T2). Flames from a grease fire ignited kitchen cabinets, eventually causing the kitchen to flashover into the attached living room. Upon fire department arrival, a fully developed fire existed in the living room and kitchen of apartment T2. Prior to exiting the apartment, the occupant opened both the rear sliding door and the apartment entrance door in an attempt to ventilate smoke from the apartment.

 

Figure 06. A typical floor plan of the right side apartments at 30 Dowling Circle.

 

An analysis of the ventilation flow path through the apartment with FDS indicated that a significant unidirectional flow path existed up the stairs with an inlet at the rear terrace sliding door and outlet at the front apartment entrance door leading to the stairwell.

Figure 7. Smokeview frame of the rear of the building indicating the fire origin and smoke spread within the T2 apartment. Figure 8. View of smoke flow out of kitchen and open sliding glass door (center of photo) in the rear of apartment T2. Figure 9. Smokeview frame of flashover of the kitchen with flames extending into the living room. Flames also begin to extend out of the rear sliding door and impact the balcony above.

 

Figure 10. Ignition of second level balcony resulting from flame extension from living room.

 

This unidirectional flow path up the stairs is difficult to combat and is often experienced during basement fires as crews attempt to descend interior stairs. The model indicates sustained air temperatures in the stairwell of approximately 600 Fahrenheit (315 Celsius) at velocities of approximately 6 mph (2.7 m/s) from floor to ceiling as crews attempted to descend the stairs. This is consistent with statements from firefighting crews, who experienced extremely high heat conditions and indicated periodically seeing flames in the smoke layer flowing up the stairs.

The elevated air velocity of the stairwell flow path resulted in a high rate of convective energy transfer to the structural firefighting gear and high perceived temperatures as the firefighters attempted to descend the stairs. Firefighting crews flowed a hoseline down the stairs to combat the high temperatures; however no significant cooling was noticed by firefighters because the hose stream could not reach the seat of the fully developed fire in the kitchen area.

The crews were simply cooling the ventilation flow path without cooling the source of the energy in the apartment. It was not until a hose stream was directed through an exterior window and a portion of the fire was extinguished that gas temperatures and velocities began to decrease, allowing firefighters to make entry to the terrace apartment via the stairs.

Figure 12. Smokeview section frame showing unidirectional flow of approximately 600 Fahrenheit (315 Celsius) gases out of the stairwell entrance door

Front photo of unidirectional flow of smoke up stairwell from apartment T2. Note the high volume of smoke from floor to ceiling as the stairwell door serves as the flow path outlet. The ground ladder in the foreground was used to rescue an occupant on the third floor trapped by heavy smoke in the stairwell. (Refer to Figure 014)

Figure 014. Front photo of unidirectional flow of smoke up stairwell from apartment T2. Note the high volume of smoke from floor to ceiling as the stairwell door serves as the flow path outlet.

 

The first arriving engine, E-11, was staffed with a Captain, Lieutenant, Driver/Operator, and a Firefighter. Upon arrival at 1820 hours, the Captain gave a brief initial report describing a three story garden apartment with smoke showing from side Alpha: “The Captain of E-11 will have Command and we are initiating an aggressive interior attack with a 1 ¾” hand line”. Command also instructed the second due engine to bring him a supply line from the hydrant. 

A female resident (victim # 1) appeared in a third floor apartment window, Alpha/Bravo side (Apt. B-1), yelled for assistance, and threatened to jump. Smoke or fire was visible from any of the third floor windows. At 1823 hours, Command advised Dispatch that he had a rescue and that he was establishing Limited Command. Fire Dispatch was in the process of upgrading the response profile to an apartment fire with rescue when the responding Battalion Chief requested that the fire box be upgraded to a fire rescue box. While the Firefighter and Lieutenant prepared for entry into the building, the Captain and Driver/Operator extended a ladder to the 3rd floor apartment window and rescued the resident. The first attempt by the Firefighter and Lieutenant to make entry into the side Alpha entrance was unsuccessful due to the extreme heat and smoke conditions.

The second due engine, E-10, arrived at 1823 with staffing of a Captain, Lieutenant, Driver/Operator, and a Firefighter. At 1823, E-10’s crew brought a 4″ supply line to E-11 from the hydrant at Deanwood Rd. and Dowling Circle and assisted the first-in crew with fire attack.

  • The Captain from E-10 conferred with Command and was instructed to advance a second 1 ¾” hand line.
  • The window to the first floor right apartment (Apt. T-2) was removed, and the second 1 ¾” line was advanced to the building by the crew of E-10.
  • Fire attack was initiated through the removed window. At 1827, Command requested a second alarm.

At this time, heat and smoke conditions just inside the front door improved enough to allow the Firefighter and Lieutenant from E-11 to make entry through the front door and into the stairwell. There they encountered heavy, thick black smoke and high heat conditions coming up the stairs from the terrace level apartment. The Lieutenant reported that the doorway to the first floor apartment was orange with fire and he had to fight his way through heavy heat and smoke conditions to attack the fire in the first floor right apartment (Apt. T-2). Entry was made approximately 3 feet into the doorway when the Firefighter’s low air alarm began to sound, and he exited the building. A member from E-10’s crew replaced the Firefighter from E-11 on the hose line.

At the same time, the Captain from E-11 proceeded to the rear of the structure to complete his initial 360 degree size up. He noted that there was fire emanating from the open sliding doors on the first floor Charlie/Delta apartment (Apt. T-2), extending to the balcony above. E-1, staffed by a Captain, Driver/Operator, and two Firefighters arrived and completed the hookup of the supply line that had been laid to the hydrant by E-10. The rest of Engine 1’s crew grabbed tools and an extension ladder and reported to the Charlie side of the building.

Figure 015 Charlie Side ( Rear) Extension

The Photo above referenced as  Figure 015 shows conditions  from rear of flames in apartment T2 and extension to the balcony above. Note the relative minimal volume of smoke as the sliding door serves as the inlet for ventilation into the apartment. The smoke and heat is flowing in from the rear, through the apartment and up the stairs.

This unidirectional flow path up the stairs is difficult to combat and is often experienced during basement fires as crews attempt to descend interior stairs.

  • The model indicates sustained air temperatures in the stairwell of approximately 600 Fahrenheit (315 Celsius) at velocities of approximately 6 mph (2.7 m/s) from floor to ceiling as crews attempted to descend the stairs.
  • This is consistent with statements from firefighting crews, who experienced extremely high heat conditions and indicated periodically seeing flames in the smoke layer flowing up the stairs.
  • The elevated air velocity of the stairwell flow path resulted in a high rate of convective energy transfer to the structural firefighting gear and high perceived temperatures as the firefighters attempted to descend the stairs.

Firefighting crews flowed a hoseline down the stairs to combat the high temperatures; however no significant cooling was noticed by firefighters because the hose stream could not reach the seat of the fully developed fire in the kitchen area.

The crews were simply cooling the ventilation flow path without cooling the source of the energy in the apartment.

It was not until a hose stream was directed through an exterior window and a portion of the fire was extinguished that gas temperatures and velocities began to decrease, allowing firefighters to make entry to the terrace apartment via the stairs.

Plan view of flow path and temperatures within the apartment. Note the location of the seat of the fire and the location of initial hose stream application down the stairs.

Figure 016

 

Photograph of hoselines being positioned at the stairwell entrance door and front window. Note the heavy smoke venting from all front openings in apartment T2. (Figure 017)

Figure 017 Alpha Side Entry Door

 

Figure 017  Hoselines being positioned at the stairwell entrance door and front window. Rapid Fire Progression Leading to Flashover of the Third LevelFlames extended upwards from the T2 apartment sliding door and ignited the rear balconies of the second and third level apartments above.
 
Fire on the second floor balcony extended into apartment A2 by failing the sliding glass door and igniting vertical plastic slat curtains that were suspended above.As crews searched within the second floor apartment, they noted seeing the burning curtains on the floor with flames extending to a nearby couch (containing polyurethane foam padding) adjacent to the sliding doorway.
 
The fire continued to grow unsuppressed and spread to a second couch as interior firefighting crews were engaged in rescuing two victims from the living room in the second floor apartment.Personnel stated that at this point fire conditions seemed to improve, suggesting that crews were making progress extinguishing the fire. (The first arriving attack crew reported that they were able to see apparatus lights through the sliding doors on Charlie side, which indicated to them that smoke and fire conditions were improving.)Truck 1, a tiller unit staffed by a Lieutenant, two Driver/Operators, and a Firefighter, arrived on side Alpha and immediately began search and rescue operations.
 
Windows on the second floor Alpha/Delta side apartment (Apt. A-2) were vented and ladders were thrown to gain access. T-8 arrived at the alley on side Charlie. E-1 extended a ground ladder to the third floor balcony on the Charlie/Bravo side of the structure (Apt. B-1), and made access to the apartment to search for additional victims.They noted fire venting from the first floor Charlie/Delta apartment (Apt. T-2) out of the sliding glass doors progressing upwards towards the balcony on the second floor.
 
Upon entering the apartment, they conducted a primary search and noted minimal heat with light smoke conditions.The crew accessed the hallway via the apartment entry door and noticed an increase in the temperature and the amount of smoke.They immediately closed the door and exited the apartment via the ground ladder.Upon exiting the apartment, E-1’s crew observed E-292 on the scene with a hand line extending into the apartment of origin, (first floor, Charlie/Delta side, Apt. T-2).
 
The officer on E-1 noted white smoke coming from the unit.Having already laid a supply line from the intersection of the alley and Deanwood Road, E-292’s crew extended a 1 ¾” hand line into the apartment of origin. Moderate fire conditions with zero visibility were encountered, and they reported feeling a great deal of heat on their knees as they crawled through the apartment.The Lieutenant and the Firefighter from Truck-1 entered Apartment A-2 via a second floor bedroom window (Alpha/Delta side) and began a search for additional victims. As they traversed the living room area they found an unconscious male resident (victim #2).
 
At 1836 hours, the Lieutenant notified Command via an urgent transmission that a victim had been located and they needed assistance with evacuation. The Lieutenant and Firefighter noted a small fire in the rear corner near the victim as they exited the room. The crew returned to the bedroom from which they had entered and closed the door behind them. Victim #2 was then evacuated from the apartment via a ground ladder through the bedroom window, and transferred to EMS personnel on side Alpha.
 
Figure 019 Flame extension and suppression efforts at the rear of the structure. Flames caused the second level glass slider to fail and ignite plastic curtains in the doorway located
 

Figure 019

 
 

The middle level apartment (A2) entrance door was opened by a second search crew around the same time as the second couch ignited, creating a ventilation flow path from the second floor balcony, through the apartment, and upwards into the stairwell (third floor). This flow path follows the same general route through the apartment and into the stairwell as was seen in the terrace level apartment below. Squad 303’s crew arrived on scene after the bulk of the fire in the terrace level apartment had been suppressed and appeared to be under control. The crew entered the front stairwell, which had minimal smoke up to the second level and the crew began to systematically search the building.

Squad 303’s crew proceeded to search two apartments before entering the third floor right side apartment to conduct a search, leaving the entrance door open. It should also be noted that carpeting impacted the bottom of the door and prevented the apartment entrance doors on the second and third levels from closing automatically. The entry doors had to be actively pushed closed to overcome the friction of the carpet.

 

Photo depicting building smoke and fire conditions around the arrival of Squad 303.

Note the lack of heavy smoke or fire in the stairwell or terrace level.

There is also no indication of the growing fire in the second (middle) level apartment.

 

 

 

When Squad 303’s crew of two firefighters entered the third level apartment (B2), smoke was banked about halfway down the walls with moderate visibility. The crew could clearly see the floor of the apartment without the need to crawl below the smoke layer to search. Squad 303’s crew was unaware of the flames spreading across the two couches in the second floor apartment below them. The crew split in order to search the apartment faster, with one firefighter searching the front bedrooms and the officer searching the kitchen and living room.

As flames in the second level began to rollover into the apartment entranceway, the smoke layer in the third level quickly dropped to the floor with a rapid increase in temperature. With Squad 303’s crew searching above, flames began to extend into the stairwell, supplied by sufficient ventilation flowing through the apartment. This combination of fuel, heat and oxygen rich fresh air resulted in a rapid increase in heat release rate and flashover of the second level apartment followed by full room involvement.

The open entrance doors on the second and third levels created a ventilation flow path through the second floor apartment, into the sealed stairwell and up through the third floor apartment directly above. The flames followed this flow path and extended from the second floor, through the stairwell and into the living room area of the third floor apartment. Flashover of the third floor occurred approximately 30 seconds after the second floor experienced flashover.

Figure 026 and 027

 

Rollover from the second level apartment into the stairwell.

 

 
 
Flames followed the ventilation flow path and extend into the third floor apartment, resulting in ignition of the couches just inside the doorway.

 

 

    

 

Command sounded the building evacuation tones as flames extended into the hallway and up to the third level apartment.

Two couches just inside the entrance door on the third level ignited, blocking the primary means of egress for both firefighters from Squad 303. Upon hearing the evacuation horns from the trucks, the second firefighter from Squad 303 (searching the front bedrooms) attempted to exit the apartment via the apartment entrance door, however he was blocked by flames in the living room and stairwell.

Trapped in the bedroom, the firefighter bailed out headfirst down a ground ladder on the front side from the third floor. Squad 303 officer’s means of egress through the apartment entrance door was also blocked by the flames in the living room and stairwell. There were no windows located in the rear of the apartment.

The only means of escape was the balcony slider, however the entire balcony was engulfed in flames from the fully involved apartment below. With both escape routes blocked by flames and experiencing extremely high heat conditions, Squad 303’s officer requested assistance and declared a MAYDAY from the rear of the third floor apartment.

Firefighters re-entered the structure to combat the fire and locate the trapped firefighter. The downed firefighter was eventually located on the third level just inside the sliding glass door and was removed to the rear balcony. The firefighter was then extricated in a stokes rescue basket down the aerial ladder of a truck located in the rear, where he was subsequently transported to the hospital.

Effects of Compartmentation on Fire Spread

The Post Incident Analysis Team requested that alternate modeling scenarios be conducted to explore the effects of compartmentation on fire spread throughout the building.

The team specifically wanted to know how the ventilation flow paths through the stairwell would differ if the second or third level apartment entry doors were shut after entering/leaving the apartments. Two alternate computer fire modeling scenarios were conducted.

The first alternative modeling run featured the exact same fire scenario, except the second (middle) level apartment door was closed after the last victim was removed from that apartment. The apartment entry doors from the stairwell were fire-rated doors constructed of solid wood.

  • As soon as the door is shut, the ventilation flow path through the apartment and up the stairwell is blocked.

 

Shutting the second level apartment door blocks the flow path and flame extension into the stairwell. 

Even with the third floor apartment door left open, the model indicates that the stairwell and third floor remain tenable for firefighters. Flames eventually extend from the third floor balcony into the apartment, however the escape routes through the stairwell and the front apartment windows are accessible.           

The model indicates that closing the second level apartment door prevents the flow of smoke, heat and other products of combustion from entering the stairwell, thus preventing flashover of the stairwell and the third level. As long as the second floor entry door remains shut, the model indicated that the conditions within the stairwell and third floor remain tenable for firefighters, even with the third floor apartment door open.

A second alternative modeling scenario was conducted where the third level entrance door was closed after crews made entry to search the apartment.The same fire conditions from the actual model were used.When the door remained closed, the outlet of the ventilation flow path was blocked at the top of the stairs. Without a complete flow path, there wasn’t sufficient oxygen flowing through the second floor apartment to support extended burning in the stairwell.

Consequently after flashover of the second floor, the flames in the stairwell only exist momentarily before consuming all available oxygen and becoming ventilation limited.The fire model indicated that temperatures within the third floor apartment stayed tenable for firefighters, even with a fully developed fire on the second floor and flames in the stairwell.

Flames would eventually extend up the rear balcony to the third level, however they would not block egress through the living room and front windows of the apartment.By closing the apartment door on the third floor and blocking the outlet for fire gases emanating from the second floor apartment, the third floor apartment remains tenable for firefighting crews and the temperatures only briefly spike in the stairwell before the fire becomes ventilation limited.The ventilation flow through the apartments results in an increased burning rate within both the second and third levels, as well as the stairwell.                     

Results of each modeling scenario describing extent of flame spread

Results of each modeling scenario describing extent of flame spread.

 
 
 
 
 
 
 
 
 
 
The Effects of Compartmentation on Fire Damage to the StructureThe impact of compartmentation on fire and smoke spread is evident by examining the post-fire damage throughout the structure. While other factors contributed to the relative fire damage, including fire department overhaul and relative apartment configuration, analyzing the damage to the building and the position of the apartment entry doors provides insight on the benefits of compartmentation.

By closing apartment unit entrance doors and interior hollow core doors, one can slow or even block the ventilation flow path through the structure, thus significantly reducing the rate of fire spread. The photos below represent the post-fire damage in all six apartments within the fire building. Four of the six apartment entry doors were open for the majority of the fire and the relative difference in damage is clearly evident.

Terrace level stairwell landing looking into T1 (left) and T2 (right) apartments.

 

Door Closed……Door Open

 

 

Using doors to compartmentalize and limit fire and smoke spread in a structure is not limited to fire-rated entrance doors. Interior hollow core doors also offer considerable protection for compartmentation purposes.

A search crew utilizing the Vent, Enter and Search (VES) technique through a front window used a hollow core bedroom door to isolate themselves from the developing fire in the living room of apartment A2.

As the crews removed the second victim from the living room to the bedroom, they shut the bedroom hollow core door behind them.

The living room soon experienced flashover followed by full room involvement, however the bedroom remained isolated from the heat and smoke for the duration of the fire. The photos below illustrate this effective use of compartmentation to protect firefighters during a search.

 
Controling the Doors during VES

 

 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
SUMMARY:
While no fire model will exactly replicate a fire, this model provided insight on the route of fire spread, the rapid fire growth leading to flashover of the second and third level, and the benefits of compartmentation on slowing fire and smoke spread.
  • The unidirectional flow path up the stairs from the terrace level apartment resulted in a high rate of convective heat transfer to the firefighters initially attempting to descend the stairs, making attacking the seat of the fire very difficult.
  • The model then supported the fact that the main stairwell acted as an open channel for fire and smoke spread between the second and third levels, resulting in flashover of the third level in approximately 30 seconds after the second level.
  • This rapid fire growth leading to flashover is supported by photographs, witness statements and fireground audio.
  • The model was then utilized to explore the effects of compartmentation using apartment entrance doors.
  • The FDS model supported the scene observations and indicated that shutting the entrance doors blocked the flow of buoyancy driven fire gases through the structure, ultimately preventing fire extension to the third floor apartment via the stairwell.
  • The FDS model was utilized as part of the overall engineering analysis of this tragic fire and allowed for a better understanding of the events that led to the firefighter MAYDAY and subsequent Line of Duty Death.
  • The model was also used as an educational tool providing insight on potential methods of preventing similar tragedies in the future.
  • The results of this engineering analysis are intended to be reviewed by the Post Incident Analysis Team to assist in the creation of recommendations to mitigate the danger associated with future fire incidents.

References:

Texas Captain; 2010 LODD Report Issued with Lessons Learned

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Captain Thomas Araguz III

 

Captain Araguz, a 30 year old, 11-year veteran of the Wharton Volunteer Fire Department made Captain in 2009. He lost his life while battling a multiple alarm fire a the Maxim Egg Farm located at 3307 FM 442, Boling, Texas on July 3, 2010.  The Texas State Fire Marshal’s Office issued the Fire Fighter Fatality Investigation Report, SFMO Case Number FY10-01 that provides a detailed examination of the incident, operations and yeilds findings and recommendations. A full version of the report is available at the Texas SFMO web site HERE.

 On July 3, 2010, Wharton Volunteer Fire Department Captain Thomas Araguz III was fatally injured during firefighting operations at an egg production and processing facility. At 9:41 PM, Wharton County Sheriff’s Office 911 received a report of a fire at the Maxim Egg Farm located at 3307 FM 442, Boling, Texas. Boling Volunteer Fire Department and the Wharton Volunteer Fire Department responded first, arriving approximately 12 minutes after dispatch. Eventually, more than 30 departments with 100 apparatus and more than 150 personnel responded. Some departments came as far as 60 miles to assist in fighting the fire.

Aerial View

 

The fire involved the egg processing building, including the storage areas holding stacked pallets of foam, plastic, and cardboard egg cartons and boxes. It was a large windowless, limited access structure with large open areas totaling over 58,000 square feet. A mixed construction, it included a two-story business office, the egg processing plant, storage areas, coolers, and shipping docks. It was primarily metal frame construction with metal siding and roofing on a concrete slab foundation with some areas using wood framing for the roof structure.

Captain Araguz responded to the scene from the Wharton Fire Station, approximately 20 miles from the fire scene, arriving to the front, south side main entrance 20 minutes after dispatch. Captain Araguz, Captain Juan Cano, and Firefighter Paul Maldonado advanced a line through the main entrance and along the south, interior wall to doors leading to a storage area at the Southeast corner.

Maldonado fed hose at the entry door as Captains Araguz and Cano advanced through the processing room. Araguz and Cano became separated from the hose line and then each other. Captain Cano found an exterior wall and began kicking and hitting the wall as his air supply ran out. Firefighters cut through the exterior metal wall at the location of the knocking and pulled him out. Several attempts were made to locate Captain Araguz including entering the building through the hole and cutting an additional hole in the exterior wall where Cano believed Araguz was located. Fire conditions eventually drove the rescuers back and defensive firefighting operations were initiated.

Captain Cano was transported to the Gulf Coast Medical Center where he was treated and released. Captain Araguz was recovered at 7:40 AM, the following morning. Initially transported by ambulance to the Wharton Funeral Home then taken to the Travis County Medical Examiner’s Office in Austin, Texas for a post-mortem examination.

Site Plan of Building Complex

Building Structure and Systems

The fire incident building was located on the property of Maxim Egg Farm, located within an unincorporated area of Wharton County. The 911 address is 580 Maxim Drive, Boling, Texas 77420.

Wharton County has no adopted fire codes, or model construction codes, and no designated Fire Marshal on staff that conducts fire safety inspections within their jurisdiction.

National Fire Protection Association (NFPA) Standard 101, Life Safety Code, 2009 Edition, is adopted by the State Fire Marshal’s Office, and is the applicable standard for fire and life safety inspections in the absence of an adopted fire code within unincorporated areas of a county by an applicable authority. All references regarding evaluation of the incident building in relation to minimum life safety requirements are based on NFPA 101, Life Safety Code, 2009 Edition.

Maxim Farm property includes 23 chicken coops known as layer barns that average 300 feet long and 50 feet wide holding between 15,000 to 25,000 chickens each. These layer barns inter-connect to a central processing building by a series of enclosed conveyor belts transporting over one million eggs daily.

  • The property includes integrated feed silos, water tanks, and waste management facilities. Additional areas on the property include equipment barns, shipping offices, loading docks, coolers, storage areas, and business offices.

 Overall Building Description

The main processing structure was an irregularly shaped mixed construction of metal, concrete block, and wood framing on a concrete slab foundation with approximately 58,000 square feet of space. Three dry-storage rooms connected by a wide hallway lined the east side of the plant. A concrete block (CMU) wall separated the egg processing area from the East Hallway and storage rooms. Coolers were located north of the processing room with the loading docks along the west side of the structure. The loading docks were accessible from the processing room, Cooler 3, and Cooler 2. Cooler 1 was located at the north end of Dry Storage 2. A two-story building housing the business office was attached to the main processing plant at the southwest corner.

Construction Features

The building construction was classified as an NFPA 220, Type II-000 construction with an occupancy classification by the Life Safety Code as Industrial with sub-classification as special-purpose use. The Life Safety Code imposes no minimum construction requirements for this type of occupancy.

The predominant use of the building was to process and package fresh eggs for shipment after arriving by automated conveyor directly from a laying house adjacent to the building. The general floor plan of the building consisted of a large egg processing room, with surrounding areas used for storage of packing materials and two large drive-in coolers for holding packaged eggs prior to shipping.

Building construction consisted of a combination of steel and wood framing with a sheet metal exterior siding and roofing over a low-pitch roof on a concrete slab foundation. Structural elements within the interior of the building were exposed and unprotected with no fire-resistance rated materials applied. The load bearing structural elements consisted of steel beams, and steel pipe columns, with steel open web trusses supporting the roof structure.

  • Wood components were also used as part of the load bearing elements and wall framing.
  • Perimeter walls of the cooler compartments were constructed of concrete masonry units (CMU).
  • The building was not separated between other areas of use by fire-resistance rated assemblies.
  • Ancillary facilities located within the building used for administrative offices and other incidental spaces were constructed of wood framing with a gypsum wallboard finish.

Detailed Construction Features

The front of the structure faced to the south where the main entrance to the processing room and business offices was located approximately 4 feet above the parking lot grade level and accessed by a series of steps. The business office was a two-story wood frame construction with a vinyl exterior siding under a metal roof on a concrete slab foundation. Additional separate, single-story, wood frame structures with offices located to the west of the main business office connected by covered walkways.

Processing Room

The egg processing room was 141 feet along the east and west walls and approximately 100 feet along the north and south walls. The processing room received the eggs transported from the layer barns on the conveyer belt system. The room contained the processing equipment and conveyor systems where eggs were cleaned, graded, packaged and moved to large coolers to await shipment. The construction of the processing room was sheet metal panels embedded into the concrete slab foundation supported by 8-inch wide metal studs. Sheet metal panels lined the exterior and interior sides of the south and west walls with fiberglass insulation sandwiched between.

Main Processing Area

The north wall separated the processing room from Cooler 3 and consisted mainly of interlocking insulated metal panels embedded into the slab locked at the top in metal channels. Their interior surface was polyurethane laminate.

The east wall was mainly of concrete block (CMU) construction. A USDA office and a mechanics room were accessed through doors in the east wall of the processing room. The northeast corner of the processing room extended into the north end of the east hallway, forming an 18 feet by 18 feet area with wood frame construction on a concrete stem wall with fiber cement board (Hardy board) and metal panel siding. A 6-feet wide opening between the processing and dry-storage areas with a vinyl strip door allowed unrestricted access.

Along the south wall of the processing room, a walkway between the processing equipment and exterior wall led to swinging double doors at the southeast corner to enter into Dry Storage 3. Conveyors carried the eggs from the north and south layer barns through openings in the walls of the extension of the processing room. The conveyors from the north and south layer barns entered the building suspended overhead. As the conveyors approached the entrance to the main processing room, they gradually descended to 3.5 feet above floor level and were supported by metal brackets attached to the floor. Electric drive motors attached to the conveyors at several points along their lengths to power their movement.

The roof consisted of steel columns and girders with metal panel roofing attached to metal purlins supported by steel rafters. Wire mesh supported fiberglass insulation under the roof deck. The roof gable was oriented north to south.

 

Dry Storage

The plant included three dry-storage rooms along the eastern side of the building connected by an east hallway. Dry Storage 1 and Dry Storage 2 were located in the northeast corner of the plant under a common sloping metal roof. The dry-storage rooms held pallets of containers including polystyrene egg crates, foam egg cartons, pulp egg cartons, and cardboard boxes.

 

Dry Storage 1 was approximately 123 feet long and 50 feet wide and was 4 feet below the grade of the rest of the plant. It was added to the east side of Dry Storage 2 in 2008. Dry Storage 1 was a concrete slab and 4-feet high concrete half wall topped with wood framing and metal siding. The metal roof sloped from 11 feet high above the west side to 10 feet high above the east wall. The roof attached to 2 inch x 8 inch wood joists supported by two rows of steel support columns and steel girders. The two rows of seven columns were oriented in a north-south direction.

A concrete ramp at the south end facilitated access to the East Hallway and Dry Storage 2 and the main level of the processing room. A concrete ramp at the northeast corner of Dry Storage 1 provided access to the rear loading dock. The rear dock was secured on the interior at the top of the ramp by a wood frame and metal double door with a wooden cross member and a chain and padlock. An additional wood frame and screened double door secured on the interior.

The conveyor belt from the north layer barns ran the length of the west side of Dry Storage 1 where it turned to the west, crossing Dry Storage 2 and the East Hallway into the main processing room.

Dry Storage 1 contained 29 rows of pallets, seven to eight pallets deep, of mainly Styrofoam egg crates stacked between 7 and 10 feet high, depending on their location. Corridors between the rows were maintained to provide access to the pallets with an electric forklift. Fluorescent light fixtures attached to the wood rafters in rows north to south with their conductors in PVC conduit. Skylights spaced evenly above the west side allowed for natural light. Pallets of stock material were single stacked below the locations of the light fixtures to keep clearance and prevent damage.

Dry Storage 2, located west of and 4 feet above Dry Storage 1, stored pallets of flattened cardboard box stock. The room was approximately 81 feet long and 40 feet wide. The south wall was the processing room extension and was approximately 25 feet long. The east side of the room was open to Dry Storage 1 with 4 inch x 4 inch unprotected wood studs spaced unevenly from 4 feet to 9 feet, supporting the metal roof. The west wall was CMU construction and was the exterior wall of Cooler 3. The metal roof sloped from the top of the west wall approximately 12 feet high to approximately 11 feet above the east side.

The room was accessed from the south end at the top of the ramp leading down into Dry Storage 1. Pallets of folded cardboard boxes were stacked along the entire length of the west wall extending 16 to 20 feet to the east. The rows of pallets were without spacing for corridors. One row of six fluorescent light fixtures attached to wood rafters near the north-south centerline.

The East Hallway was approximately 118 feet long and 37 feet wide running along the length of the east side of the processing room. The East Hallway connected Dry Storages 1 and 2 with Dry Storage 3 by a corridor at the south end. The East Hallway allowed access between the storage room areas and into utility rooms including the Boiler Room at the north end and a mechanics room and small utility closet. Pallets of polystyrene egg crates were stored along the east wall in rows of three pallets each. Seven pallets of polystyrene egg crates were stored along the conveyors.

The west wall was concrete block construction (CMU) until it connected to the extension of the processing area constructed of wood frame covered by Hardy board and sheet metal. The east wall was sheet metal embedded in the concrete slab supported by 2 inch x 4 inch wood studs with Hardy board interior. The metal roof sloped from a height at 12 feet at the west wall to 10 feet high at the east wall, supported by 4 inch x 6 inch wood columns and 2 inch x 8 inch wood joists.

Two conveyors entered the south end of the east hallway from Dry Storage 3. The conveyors ran parallel for approximately 80 feet along the west wall and entered the processing room through openings in the extension at the north end of the east hallway. They were 6 feet from the west wall and gradually descended from a height of 9 feet at the south end to 3.5 feet at the north. Each conveyor was 31 inches wide and combined was approximately 7 feet wide. Two compressor machines and a pressure washer were located along the west wall near the south end.

The Boiler Room, located at the northeast corner of the East Hall, housed two propane fired boilers, a water treatment system and two vacuum pumps. It was wood frame construction with metal siding under a metal roof on a combination concrete slab and concrete pier and wood beam foundation. A small utility room with service panels was constructed of concrete block on a concrete slab under a metal roof and was also located along the west wall of the East Hallway. An approximately 10 feet wide corridor connected the East Hallway to Dry Storage 3.

Dry Storage 3 extended south from the main processing room and East Hallway to the south dock area where tractor-trailers parked to unload the pallets of supplies. Two parallel conveyors suspended 9 feet overhead from the roof extended along the length of the east wall where it passed through the south wall toward the south layer houses.

The plant’s main power conductors entered the west wall of Dry Storage 3 from load centers and transformers mounted to the slab outside approximately 15 feet south of the main processing room exterior wall. Stacks of wood pallets were stored in Dry Storage 3. Corridors wide enough for forklifts provided access to the south cargo dock area.

Fire Ground Operations and Tactics

Note: The following sequence of events was developed from radio transmissions and firefighter witness statements. Those events with known times are identified. Events without known times are approximated in the sequence of the events based on firefighter statements regarding their actions and/or observations. A detailed timeline of radio transmissions is included in the appendix.

On July 3, 2010, at 21:41:10, Wharton County Sheriff’s Office 911 received a report of a fire at the Maxim Egg Farm located on County Road 442, south of the city of Boling, Texas. The caller, immediately transferred to the Wharton Police Department Dispatch, advised there was a “big fire” in the warehouse where egg cartons were stored. Boling Volunteer Fire Department was dispatched and immediately requested aid from the Wharton Volunteer Fire Department. Wharton VFD became Command as is the usual practice for this county.

Wharton Assistant Chief Stewart (1102) was returning to the station having been out on a response to a vehicle accident assisting the Boling Volunteer Fire Department when the call came in for the fire. He responded immediately and at 21:50 reported seeing “heavy fire” coming from the roof at the northeast corner of the building as he approached the plant from the east on County Road 442. When he arrived he was eventually directed to the east side of the building (D side) to the rear loading dock. Asst. Chief Stewart worked for several minutes with facility employees to gain access to the fire building before being led to the northeast loading dock.

An employee directed him on the narrow caliche drive behind the layer barns and between the waste ponds to the loading dock. Wharton Engine 1134 followed 1102 to the east side and backed into the drive leading to the loading dock. Asst. Chief Stewart’s immediate actions included assessing the extent of the fire on the interior of the building by looking through the doors at the loading dock to Dry Storage 1. Unable to see the fire through the smoke at the doors of the loading dock, an attack was eventually accomplished by removing a metal panel from the east exterior wall of Dry Storage 1 and using one 1¾”-inch cross lay. After a few minutes, the deck gun on Engine 1134 was utilized, directing water to the roof above the seat of the fire near the south end of Dry Storage 1.

Water supply became an immediate concern and 1102 made efforts to get resources for resupply. Requests for mutual aid to provide water tankers were made to area communities. During the incident, re-supplying tankers included a gravity re-fill from the on-site water supply storage tanks and from fire hydrants in the City of Boling, 3 miles from the scene and the City of Wharton, nearly 11 miles. The City of Boling water tower was nearly emptied during the incident.

The radio recording indicates there were difficulties accessing the location of the fire as apparatus were led around the complex by multiple employees. Heavy rains during the previous week left many roadways muddy and partially covered with water, which added to problems with apparatus access. In addition, fire crews were not familiar with the layout of the facility and there are no records of pre-fire plans. Asst. Chief Stewart worked for several minutes with facility employees to gain access to the fire building before being led to the northeast loading dock.

Wharton Fire Chief Bobby Barnett (1101) arrived on scene at 21:56:14, and ordered incoming apparatus to stage until he could establish an area of operations at the front, south side of the plant (A side). Chief Barnett directed Engine 1130 to position approximately 50 feet from the front main entrance of the plant. At 22:09:16, Chief Barnett (1101) established a command post on A side and became the Incident Commander; 1101 directed radio communications for the fireground to be TAC 2 and called for mutual aid from the Hungerford and El Campo Fire Departments. Chief Barnett described the conditions on side A as smoky with no fire showing. Light winds were from the east, side D, pushing the smoke toward the area of the processing room, and the front, side A, of the building.

Maxim Egg Farm Manager David Copeland, a former Wharton VFD Chief, advised Command and firefighters that the fire was in the area of the Boiler Room and should be accessed by breaching an exterior wall in the employee break area. Chief Barnett ordered Wharton crews to the breach attempt. Captain Thomas Araguz III, Captain John Cano and Firefighter Paul Maldonado were involved with this operation. The crews working in this area were in full structural personnel protective clothing and SCBA.

At 22:10, Command ordered Engine 1130 and Tanker 1160 to set up at the front entrance using Tanker 1160 for portable dump tank operations for water re-supply.

On D side, difficulty accessing the fire from the exterior of the building was reported by Asst. Chief Stewart and the crews. Heavy doors, locked loading dock doors and steel exterior paneling, required the crews to spend extra time forcing entry.

At 22:17:23, Wharton County Chief Deputy Bill Copeland (3122), once a Wharton FD volunteer firefighter, notified Command that the fire was now through the roof over Dry Storage 1.

Chief Barnett noticed smoke conditions improving at the main plant doorway and ordered crews to advance lines into the processor room. Chief Barnett stated he assigned Captain Araguz, Captain Cano and Firefighter Maldonado because they were the most experienced and senior crews available.

Positive Pressure Ventilation (PPV) was in place at the main entry door when Captain Cano, Captain Araguz and Firefighter Maldonado entered the structure into the processing room. There are no radio transmissions to verify exact entry times.

Captain Cano stated that an employee had to assist fire crews with entry into the main plant through a door with keypad access. Captain Cano reported the door to processing was held open by a three-ring binder that he jammed under the door after entry. Cano stated there was low visibility and moderate heat overhead. Captain Cano and Captain Araguz made entry on a right-hand wall working their way around numerous obstacles. The line was not yet charged and they returned to the doorway and waited for water. Wharton Engine 1130’s driver reported in his interview that he had difficulty establishing a draft from the portable tank later determined to be a linkage failure on the priming pump. 1160 connected directly to 1130 and drafted from the folding tank.

As the crew entered into the structure through the main entry door, several plant employees began entering into the administration offices through the area of the main entry door to remove files and records. This was reported to Command at 22:23 and after several minutes Chief Barnett ordered employees to stay out of the building and requested assistance from the Sheriff’s Office to maintain scene security.

At 22:31, once the line was charged, the two captains continued into the processor on the right wall leaving Maldonado at the doorway to feed hose. Captain Cano was first with the nozzle and described making it 20 feet into the building.

Cano states in his interview that he advised Command over the radio that there was high heat and low visibility, although the transmission is not recorded. Cano also reported in his interview, he could not walk through the area and had to use a modified duck walk. Cano projected short streams of water towards the ceiling in a “penciling” motion and noted no change in heat or smoke conditions. They advanced until the heat became too great and they retreated towards the center of the processor. Cano stated that they discussed their next tactic and decided to try a left-handed advance.

At 22:33, Chief Barnett advised, “advancing hose streams in main building to try to block it.”

Captain Araguz took the nozzle and Captain Cano advanced with him holding onto Araguz’ bunker gear. The crew advanced along the south wall of the processing room toward the double doors to Dry Storage 3 and lost contact with the hose line.

The investigation found the couplings between the first and second sections of the hose lodged against a threaded floor anchor (see photo) preventing further advancement of the line. How the team lost the hose line remains uncertain.

Captain Cano stated in his interview that Captain Araguz told him to call a Mayday. Captain Cano stated that he was at first confused by the request, but after some time it became apparent they lost the hose line. Captain Cano reported calling Mayday on the radio but never received a reply. Captain Cano now believes he may have inadvertently switched channels at his previous transmission reporting interior conditions. Captain Araguz had a radio but it was too damaged to determine operability. There are no recorded transmissions from Captain Araguz.

At 22:37, Deputy Chief Copeland advised Command that the fire had breached a brick wall and was entering the main packing plant. Command responded that there was a hose team inside.

At 22:42:50, Command radioed “Command to hose team 1, Cano.” This was the first of several attempts to contact Captain Cano and Captain Araguz. At 22:47:17, Command ordered Engine 1130 to sound the evacuation horn. At 22:50:44, Command announced Mayday over the radio, stating “unlocated fireman in the building.”

  • Captain Cano stated in his interview that they made several large circles in an attempt to locate the fire hose.
  • Cano became entangled in wiring, requiring him to doff his SCBA.
  • After re-donning his SCBA, Captain Cano noted he lost his radio, but found a flash light. He remembered that his low air warning was sounding as he and Araguz searched for the hose. Cano stated that they made it to an exterior wall and decided to attempt to breach the wall. Working in near zero visibility,
  • Captain Cano reported losing contact with Captain Araguz while working on breaching the wall.
  • Shortly after he lost contact, Captain Cano ran out of air and removed his mask. Captain Cano continued working to breach the exterior wall until he was exhausted.

At 22:54, crews working on the exterior of the building near the employee break area reported hearing tapping on the wall in the area of the employee break room.

  • Crews mustered tools and began to cut additional holes through the building exterior.
  • After making two openings, Captain Cano was located and removed from the building.
  • Captain Cano reported that Captain Araguz was approximately 15 feet inside of the building ahead of him.
  • Firefighters made entry through the exterior hole but were unsuccessful in locating Captain Araguz. Cano was escorted to the folding water tank and got into the tank to cool down.

Rapid Intervention Crews (RIC) were established using mutual aid members from the Hungerford and El Campo Fire Departments. The first entry made was at the main entry door where Firefighter Maldonado was located. Maldonado was relieved and escorted to the ambulance for rehab. An evacuation horn sounded and the first RIC abandoned the interior search and exited the building.

A rescue entry by a second RIC was through the breached wall of Dry Storage 3. After several minutes inside, the evacuation signal sounded due to the rapidly spreading fire and deteriorating conditions. Two additional RICs entered the structure through the loading dock doors of Dry Storage 3. Chief Barnett states that there were a total of four RICs that made entry after the Mayday. After approximately 45 minutes, all rescue attempts ceased.

As the fire extended south toward Dry Storage 3, smoke conditions became so debilitating that Chief Barnett ordered all crews staged near the front of the building on side A to move back and apparatus to relocate. Command assigned Chief Hafer of the Richmond Fire Department to “A” side operations and defensive operations were established. Captain Cano and Firefighter Maldonado were transported to Gulf Coast Medical Center and treated for smoke inhalation.

Fire ground operations continued through the night. Captain Araguz was recovered at approximately

07:40 AM. Command transferred to the Richmond Fire Department Chief Hafer at approximately

07:56 AM as 1101 and the Wharton units escorted Captain Araguz from the scene. All Wharton units cleared the scene at 08:02 AM.

Captain Araguz was transported to the Travis County Medical Examiner’s Office for autopsy. The Travis County Medical Examiner’s Office performed post mortem examinations on July 4, 2010. Captain Araguz died from thermal injuries and smoke inhalation.

Findings and Recommendations

  • Recommendations are based upon nationally recognized consensus standards and safety practices for the fire service.
  •  
  • All fire department personnel should know and understand nationally recognized consensus standards, and all fire departments should create and maintain SOGs and SOPs to ensure effective, efficient, and safe firefighting operations.

There were several factors that, when combined, may have contributed to the death of Captain Araguz. It is important that we honor him by learning from the incident.

  • Water supply became an immediate concern.
  • Although there are two water storage tanks on the facility with the combined capacity of nearly 44,000 gallons, refilling operations to tankers were slow, accomplished by gravity fill through a 5-inch connection.
  • A fire department connection attached to the plant’s main water supply pump and plant personnel familiar with the system could have sped up the refilling process at the plant.
  • Most tankers were sent to hydrants in the City of Boling 3 miles away, which in turn quickly depleted the city water supply.
  • Other tanker refilling was accomplished at hydrants on the City of Wharton water system, as far as 15 miles away.

Fire protection systems are not required by National Fire Protection Association (NFPA) Standard 101, Life Safety Code, 2009 Edition for this classification of facility. Fire sprinkler and smoke control systems may have contained the fire to one area, preventing the spread of fire throughout the plant.

Findings and recommendations from this investigation include:

 

FINDING 1:

There were no lives to save in the building. An inadequate water supply, lack of fire protection systems in the structure to assist in controlling the spread of the smoke and fire, and the heavy fire near the windward side facilitated smoke and fire spread further into the interior and toward “A” side operations. Along with the size of the building, the large fuel load, and the time period from fire discovery, interior firefighters were at increased risk.

Recommendation: Fire departments should develop Standard Operating Guidelines and conduct training involving risk management and risk benefit analysis during an incident according to Incident Management principles required by NFPA 1500 and 1561.

The concept of risk management shall be utilized on the basis of the following principles:

(a)  Activities that present a significant risk to the safety of personnel shall be limited to situations where there is a potential to save endangered lives

(b) Activities that are routinely employed to protect property shall be recognized as inherent risks to the safety of personnel, and actions shall be taken to reduce or avoid these risks.

(c) No risk to the safety of personnel shall be acceptable where there is no possibility to save lives or property.

(d) In situations where the risk to fire department members is excessive, activities shall be limited to defensive operations. NFPA 1500 Chapter 8, 8.3.2

NFPA 1500 ‘Standard on Fire Department Occupational Safety and Health Program’, 2007 ed., and NFPA 1561’Standard on Emergency Services Incident Management System’, 2008 ed. Texas Commission on Fire Protection Standards Manual, Chapter 435, Section 435.15

(b)  The Standard operating procedure shall:

(1) Specify an adequate number of personnel to safely conduct emergency scene operations;

(2) limit operations to those that can be safely performed by personnel at the scene;

FINDING 2:

Initial crews failed to perform a 360-degree scene size-up and did not secure the utilities before operations began.

Recommendation: Fire departments should develop Standard Operating Guidelines that require crews to perform a complete scene size-up before beginning operations. A thorough size up will provide a good base for deciding tactics and operations. It provides the IC and on-scene personnel with a general understanding of fire conditions, building construction, and other special considerations such as weather, utilities, and exposures. Without a complete and accurate scene size-up, departments will have difficulty coordinating firefighting efforts.

Fireground Support Operations 1st Edition, IFSTA, Chapter 10 Fundamentals of Firefighting Skills,

NFPA/IAFC, 2004, Chapter 2  

FINDING 3

The Incident Commander failed to maintain an adequate span of control for the type of incident. Safety, personnel accountability, staging of resources, and firefighting operations require additional supervision for the scope of incident. Radio recordings and interview statements indicate the IC performing several functions including: Command, Safety, Staging, Division A Operations, Interior Operations and Scene Security.

Recommendation: Incident Commanders should maintain an appropriate span of control and assign additional personnel to the command structure as needed. Supervisors must be able to adequately supervise and control their subordinates, as well as communicate with and manage all resources under their supervision. In ICS, the span of control of any individual with incident management supervisory responsibility should range from three to seven subordinates, with five being optimal. The type of incident, nature of the tasks, hazards and safety factors, and distances between personnel and resources all influence span-of-control considerations.

U.S. Department of Homeland Security – Federal Emergency Management Agency Incident Command Systems http://www.fema.gov/emergency/nims/ICSpopup.htm#item5 NFPA 1500 Standard on Fire Department Occupational Safety and Health Program, Chapter 8, 2007 ed.

 

FINDING 4

The interior fire team advanced into the building prior to the establishment of a rapid intervention crew (RIC).

Recommendation: Fire Departments should develop written procedures that comply with the Occupational Safety and Health Administration’s Final Rule, 29 CFR Section 1910.134 (g) (4) requiring at least two fire protection personnel to remain located outside the IDLH (Immediate Danger to Life or Health) atmosphere to perform rescue of the fire protection personnel inside the IDLH atmosphere. One of the outside fire protection personnel must actively monitor the status of the inside fire protection personnel and not be assigned other duties. NFPA 1500 8.8.7 At least one dedicated RIC shall be standing by with equipment to provide for the rescue of members that are performing special operations or for members that are in positions that present an immediate danger of injury in the event of equipment failure or collapse.

U.S. Occupational Safety and Health Administration Respiratory Protection Standard, CFR 1910.134 (g) (4); Texas Commission on Fire Protection Standards §435.17 – Procedures for Interior Structure Fire Fighting (2-in/2-out rule) NFPA 1500 Standard on Fire Department Occupational Safety and Health Program, Chapter 8, 2007 ed. NFPA 1720 Standard on Organization and Deployment Fire Suppression Operations by Volunteer Fire Departments, 2004 ed.  

FINDING 5

The interior team and Incident Commander did not verify the correct operation of communications equipment before entering the IDLH atmosphere and subsequently did not maintain communications between the interior crew and Command. Although Chief Barnett stated he communicated with Captain Cano, there was no contact with Captain Araguz.

Recommendation: Fire Departments should develop written policies requiring the verification of the correct operations of communications equipment of each firefighter before crews enter an IDLH atmosphere. Fire Departments should also include training for their members on the operation of communications equipment in zero visibility conditions.

U.S. Occupational Safety and Health Administration Respiratory Protection Standard, CFR 1910.134(g)(3)(ii) NFPA 1500 Standard on Fire Department Occupational Safety and Health Program, Chapter 8, 2007 ed.

 

FINDING 6

The interior operating crew did not practice effective air management techniques for the size and complexity of the structure. Interviews indicate the crew expended breathing air while attempting to breach an exterior wall for approximately 10 minutes, then advanced a hose line into a 15,000 square feet room without monitoring their air supply. During interviews Captain Cano estimated his consumption limit at 15 – 20 minutes on a 45 minute SCBA.

Recommendation: Crews operating in IDLH atmospheres must monitor their air consumption rates and allot for sufficient evacuation time. Known as the point of no return, it is that time at which the remaining operation time of the SCBA is equal to the time necessary to return safely to a non-hazardous atmosphere. The three basic elements to effective air management are:

  • Know your point of no return (beyond 50 percent of the air supply of the team member with the lowest gauge reading).
  • Know how much air you have at all times.
  • Make a conscious decision to stay or leave when your air is down to 50 percent.

IFSTA [2008]. Essentials of Fire Fighting and Fire Department Operations, 5th ed., Chapter 5, Air Management, page 189 Fundamentals of Firefighter Skills, 2nd edition, NFPA and International Association of Fire Chiefs, Chapter 17, Fire Fighter Survival.

 

Finding 7

Captains Araguz and Cano became separated from their hoseline. While it is unclear as to the reason they became separated from the hose line, interviews with Captain Cano indicate that while he was finding an exterior wall and took actions to alert the exterior by banging and kicking the wall, he lost contact with Captain Araguz.

**Captain Cano credits his survival to the actions he learned from recent Mayday, Firefighter Safety training.

Recommendation: Maintaining contact with the hose line is critical. Losing contact with the hose line meant leaving the only lifeline and pathway to safety. Team integrity provides an increased chance for survival. All firefighters should become familiar with and receive training on techniques for survival and self-rescue.

United States Fire Administration’s National Fire Academy training course “Firefighter Safety: Calling the Mayday” Fundamentals of Firefighter Skills, 2nd edition, NFPA and International Association of Fire Chiefs, Chapter 17, Fire Fighter Survival.

Additional References Related to Surviving the Mayday and RIT operations from 2011 Safety Week at CommandSafety.com;

Day One: Fire/EMS Safety, Health & Survival Week 2011: Day One- Are You Ready?

Day Two: Fire/EMS Safety, Health and Survival Week: Day Two- Building Knowledge = Fire Fighter Safety

Day Three: Fire/EMS Safety, Health and Survival Week: Day Three-The New Rules of Engagement

Day Four: Fire/EMS Safety, Health and Survival Week: Day Four -The New Fire Ground

Day Five: Fire/EMS Safety, Health and Survival Week 2011: Day Five: Near-Misses, Maydays and Floor Collapses

Day Six: Fire/EMS Safety, Health and Survival Week 2011, Day Six; From Waldbaum’s to Hackensack-Worcester to Charleston; Legacies for Operational Safety

Day Seven: Fire/EMS Safety, Health and Survival Week 2011, Day Seven; Fire Fighter, Fire Officer and Command Training and Preparedness

Day Eight Plus One: Mayday and Rapid Intervention Realities: The Phoenix Perspective

188 Days of Opportunity to make a Difference: Surviving the Fire Ground

Other Links:

Mayday and Rapid Intervention Realities: The Phoenix Perspective

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Southwest Supermarket Fire March 14, 2001

This year’s Fire/EMS Safety, Health and Survival Week focused on Surviving the Fire Ground: Fire Fighter, Fire Officer and Command Preparedness. One of the major objectives of this year’s theme was addressing a variety of functional areas for the Mayday event. For many of you, the conditions, outcome and lessons learned from the Southwest Supermarket Fire, maydays and the Line of Duty Death of Phoenix (AZ) firefighter Bret Tarver in 2001 are as fresh today as they were ten years ago and certainly as relevant as when many of us first read the Final Report issued by the Phoenix FD.

However, to many others in the Fire Service the Bret Tarver LODD and the Southwest Supermarket fire along with the lessons learned that were identified and the research that was instituted may not have made it onto your radar screen. In this the final days of the 2011 Fire/EMS Safety week, it is very appropriate to provide some insights on this mayday event and more importantly provide you with the opportunty to learn from the past, to understand operational parameters, capabilites, fallacies, misconceptions and limitations when we talk about Mayday, RIT and FAST activities and operational deployments.

Here’s an overview of the event;

On March 14, 2001 the Phoenix (AZ) Fire Department lost firefighter Brett Tarver at the Southwest Supermarket fire.

In that event, it was 5:00 in the afternoon, the grocery store was full of people and fire was extending through the building. Phoenix E14 was assigned to the interior of the structure to complete the search, get any people out, and attempt to confine the rapidly spreading fire to the rear of the structure. Shortly after completing their primary search of the building the Captain decided it was time to get out. Tarver and the other members of Engine 14 were exiting the building when Tarver and his partner got lost.

The engineer (driver) was leading the group following the attack line they had brought into the supermarket fire, followed by Tarver and his partner, with the company officer being the last person to begin the long crawl out of the smoke filled structure. At some point Tarver and his partner got off the hose line and moved deeper in the supermarket fire away from their only exit. Early on during the exit attempt through maze like conditions Tarver and his partner basically turned left instead of right. Not knowing this the company officer continued to crawl out of the building thinking his whole crew was ahead of him on the attack line. Tarver and his partner crawled deeper into the fire occupancy eventually ending up in the butcher shop area where they eventually became separated.

Based on radio reports of deteriorating conditions inside the building from E14 and other companies the Incident Commander (IC) considered a switch to a defensive strategy and started the process of pulling all crews out of the structure. During this process Tarver radioed the IC telling him that he was lost in the back of the building. The IC deployed two companies as Rapid Intervention Crews (RICs) through the front access point to no avail.
Other companies coming to their rescue through the back room area of the supermarket later rescued Tarver’s partner. After several unsuccessful rescue attempts, Tarver succumbed to carbon monoxide poisoning from the acrid smoke and was eventually removed from the building as a full code. Trying to remove the 260-pound firefighter was nearly impossible for rescue team members. Outside, the resuscitation efforts failed.

During the rescue efforts there were more than twelve (12) mayday’s issued by firefighters trying to make the rescue. On this tragic day, one other firefighter (attempting to rescue Tarver) was removed in respiratory arrest and was later resuscitated by fire department paramedics on the scene.

Over the next year (The Recovery), the department systematically reviewed its standard operating procedures and fireground operational activities at the strategic (command), tactical (sector) and task (company) levels of the entire organization in an attempt to prevent such a tragic event from ever happening again to the Phoenix Fire Department. One of the many significant questions that was asked was why didn’t the rapid intervention concept work? Immediately after the fire the Phoenix Fire Department reviewed its Rapid Intervention and Mayday standard operating procedures (SOPs). Based on drills, training and the data acquired through those drills, in the year following the incident the standard concept of a rapid intervention is now being challenged.

It is now evident that rapid intervention isn’t rapid. (Reference: Excerpts from the original article by Steve Kreis and FireTimes.com, LLC. http://www.firetimes.com/printStory.asp?FragID=8399 )

In the wake of the 2001 Southwest Supermarket Fire and LODD of FF Brett Tarver, the Phoenix (AZ) Fire Department issued a comprehensive report of the incident and the lessons learned and research conducted by the FD.

Beyond 2011 Fire/EMS Safety, Health and Survival Week; Fire Fighter, Fire Officer and Command Training and Preparedness

  • If you have never heard about the Southwest Supermarket Fire and the Bret Tarver LODD and incident and never read the report;
    • take the time to do so and understand that the concepts of RIT and FAST are made up of far more elements, considerations and more importantly realities of what you think you can do versus what you may actually be able to do.
    • if you’ve read it in the [past], take a few minutes to review and refresh;
    • see where your organization, department and RIT/FAST training and capabilities are today-
    • what are the capabilities of your fire fighters, officers and commanders?
  • Take a look at the NIOSH report and the recommendations contained; how does your deparment stack up today?
  • After reading the reports, take a close look at your organization, your personnel and your training and your capabilities and
  • ask yourself if you are truly able to perform the necessary RIT/FAST operations or
  • do you have a ways to go to better prepare, train and ensure you’re able to undertake the job and address the fireground survival needs when a mayday is called.
  • did you take the time during this safety week to make some progress, identify some new insights, gaps or renewed interests and desire to enhance on your capabilities and strengths?
  • Are your Mayday, RIT and FAST capabilites, skills and knowledge better today in 2011 than they were in 2001?

 

References:

The following is an article piece posted by my good friend Mike Ward and posted a number of years ago from www.thewatchdesk.com written by: Mike Ward

Rapid Intervention Reality – from Phoenix
 

Subject: Rapid Intervention Reality Check By Michael Ward   

The Phoenix Fire Department’s Deployment Committee has a sobering message to their firefighters operating in large buildings, like a 7,500 square foot warehouse: “If you extend an attack line 150′, get 40 feet off the line and then run out of air, it will take us 22 minutes to get you out of the structure.” The lesson to remember is not to get off the fire attack line.  The statement is based on 200 rapid intervention drills conducted by PFD as part of their recovery process after Firefighter/paramedic Brett Tarver  died in the March 14, 2001 Southwest Supermarket fire.

PFD obtained three vacant commercial buildings: a warehouse, a movie theatre and a country-western bar. The RIT drill was for the first alarm companies to respond to a report of two firefighters in trouble. One is disoriented and the other one is unconscious. The buildings were sealed from outside light and the facemasks were obscured to simulate heavy smoke conditions. The RIT teams were equipped and deployed as if this is was a working fire. The department ran through about 200 RIT drills with 1144 PFD firefighters participating. Their activities were monitored and timed. An Arizona State University statistician analyzed the data.

The results show that rapid intervention is not rapid:

  • Rescue crew ready state 2.50 minutes
  • Mayday to RIC entry 3.03 minutes
  • RIC contact with downed firefighter 5.82 minutes
  • Total time inside building for each RIC team 12.33 minutes
  • Total time for rescue 21 minutes

The evolutions also revealed three consistent ratios:

  • It takes 12 firefighters to rescue one
  • One in five RIC members will get into some type of trouble themselves.
  • A 3000-psi SCBA bottle has 18.7 minutes of air (plus or minus 30%)
     

The results of the RIC drills reflects the experience Phoenix had during the efforts to rescue Firefighter/paramedic Brett Tarver. There were a dozen maydays sounded during the rescue effort, and one PFD firefighter was removed from the supermarket in respiratory arrest.

The Phoenix experience is not unique. Houston Fire Chief Chris Connealy participated in a discussion about the Phoenix RIC drills during the 2003 Change in the Fire Service Symposium. On October 13, 2001, Houston Engine 2 Captain Jay Jahnke died on the fifth floor of Four Leaf Towers, a 41 story residential high-rise. During the Houston RIC operation, two heavy rescue company firefighters became disoriented, low on air and had to rescue themselves. An engine company captain and firefighter run out of air and collapsed on the fire floor. Chief Connealy said that the Houston experience is similar to Phoenix.

Phoenix is changing its approach to rapid intervention crews in three procedural ways: increase suppression units assigned to RIC, increased in command officers, and considering a two-part RIC process.

There is a scalar approach to RIC dispatch assignments in Phoenix. For a “3-1 Assignment” (three engines and one ladder), a fourth engine and an ems transport (rescue) is added to the assignment to function as the rapid intervention team. For a 1st alarm assignment, two engines, one ladder, one rescue and a battalion chief are the RIC team. A second alarm includes an additional two engines and ladder for RIC. Beyond a second alarm, the incident commander can call additional companies as needed.

The recovery process also looked at the utilization of company and command officers on the fireground. A company officer core competency is to command a fire company. A core chief officer competency is to command fire companies. It is a function of the fire department hierarchical structure, not of personality.  For example, a captain filling-in as a battalion chief does a better job as a West Sector officer than she would have if she was commanding Engine 2 AND in charge of West Sector. At the sector level of the incident management system, company officers are required to wear two hats. There are too many levels of tasks. Phoenix suggests that it would be more effective to send more command officers to a fire event to function as sector and division commanders and allow the company officers to command their companies. It is a waste of talent and experience to allow command officers to stay in their fire stations while a low-frequency, high risk event like a structure fire is occurring
in the city.

A third change in rapid intervention crews is using a two-phase approach.  Many of the RIC team members ran out of air during the training evolutions.  The drills showed that a 3000-psi SCBA bottle was good for 13.09 to 24.31 minutes of air. The average SCBA time was 18.7 minutes. The average time from mayday to removal was 21 minutes. RIC teams were running out of air during the firefighter removal phase. In addition, it was taking a crew of 12 firefighters to remove one firefighter. Phase one of a RIC response is to send a team in to locate the firefighters in trouble. Once located, a second RIC team enters to remove the firefighter.

You are welcome to share this with everyone. Please include the following: taken from www.thewatchdesk.com written by:
Michael Ward, Fire Science Program Head, Northern Virginia Community College.  

 

 Other recent postings and references from CommandSafety.com

Day One: Fire/EMS Safety, Health & Survival Week 2011: Day One- Are You Ready?

Day Two: Fire/EMS Safety, Health and Survival Week: Day Two- Building Knowledge = Fire Fighter Safety

Day Three: Fire/EMS Safety, Health and Survival Week: Day Three-The New Rules of Engagement

Day Four: Fire/EMS Safety, Health and Survival Week: Day Four -The New Fire Ground

Day Five: Fire/EMS Safety, Health and Survival Week 2011: Day Five: Near-Misses, Maydays and Floor Collapses

Day Six: Fire/EMS Safety, Health and Survival Week 2011, Day Six; From Waldbaum’s to Hackensack-Worcester to Charleston; Legacies for Operational Safety

Day Seven: Fire/EMS Safety, Health and Survival Week 2011, Day Seven; Fire Fighter, Fire Officer and Command Training and Preparedness

Fire/EMS Safety, Health and Survival Week 2011, Days One thru Seven;Training and Preparedness

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Did you remember to participate in the 2011 Fire/EMS Safety, Health and Survival Week?

The International Association of Fire Chiefs (IAFC) and the International Association of Fire Fighters(IAFF) were formative in developing this year’s  2011 Fire/EMS Safety, Health and Survival Week (also known as Safety Week)which commences today, June 19th and ends on June 25th. ( Week of June 19-25, 2011)

The message this year is: Surviving the Fire Ground – Fire Fighter, Fire Officer and Command Preparedness

Safety, Health and Survival Week (Safety Week) is a collaborative program sponsored by the IAFC and the IAFF, coordinated by the IAFC’s Safety, Health and Survival Section and the IAFF’s Division of Occupational Health, Safety and Medicine, in partnership with more than 20 national fire and emergency service organizations.

We’ve got a whole lot of resources, links and daily commentary and articles that were posted on each day of SAfety Week over at CommandSafety.com

If you didn’t have a look and read, take some time to do so. If you didn’t do anything during Safety Week, there’s always next week or the week after… find the time and commit to some training, insights, dialog, discussion…Get Prepared.

Day One: Fire/EMS Safety, Health & Survival Week 2011: Day One- Are You Ready?

Day Two: Fire/EMS Safety, Health and Survival Week: Day Two- Building Knowledge = Fire Fighter Safety

Day Three: Fire/EMS Safety, Health and Survival Week: Day Three-The New Rules of Engagement

Day Four: Fire/EMS Safety, Health and Survival Week: Day Four -The New Fire Ground

Day Five: Fire/EMS Safety, Health and Survival Week 2011: Day Five: Near-Misses, Maydays and Floor Collapses

Day Six: Fire/EMS Safety, Health and Survival Week 2011, Day Six; From Waldbaum’s to Hackensack-Worcester to Charleston; Legacies for Operational Safety

Day Seven: Fire/EMS Safety, Health and Survival Week 2011, Day Seven; Fire Fighter, Fire Officer and Command Training and Preparedness

The Exceptional and Noble Qualities of one Brother Firefighter

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Firefighter Mark Falkenhan

Thousands of mourners from across the state of Maryland and the nation arrived at Cathedral of Mary Our Queen in North Baltimore (MD) on Monday January 24th to honor fallen firefighter Mark Falkenhan

The call for the fire at 30 Dowling Circle came in to fire dispatchers at 6:18 p.m. The call came in as a kitchen fire; however, fire investigators have not determined that the fire originated in the kitchen. The fire remains under investigation. Fire Chief John Hohman has asked the federal Bureau of Alcohol, Tobacco and Firearms for assistance. Engine 11 was the first-arriving engine. The fire quickly escalated to a second-alarm, and eventually four alarms worth of equipment were dispatched. About 30 pieces of fire equipment and 100 fire personnel responded.

Mark Falkenhan arrived with the Lutherville Volunteer Fire Co. and entered the building with his partner, Dennis Fulton. At some point, Falkenhan called a mayday, indicating he was in distress. He was on the third floor, searching for fire victims. His partner was able to escape through a window on the third floor. FF Fulton escaped by diving off the balcony and sliding face-first down a ladder. Firefighters found Falkenhan on the third floor and moved him to the balcony, where crews delivered him to paramedics. Medic personnel administered advanced life support measures and transported him to St. Joseph Medical Center.

 They were on the third floor when it’s believed they were suddenly overwhelmed by a  possible flashover. Firefighter Falkenhan did not make it out. 

He signaled a “Mayday” distress call at 6:47 p.m., and rescue workers rushed to return to the third floor. They pulled Falkenhan out of the building and down the ladder, then performed advanced life-support measures. He was transported to St. Joseph Medical Center, where he was pronounced dead.

More than 200 fire trucks and an estimated 3,000 mourners—including Gov. Martin O’Malley and Baltimore County Executive Kevin Kamenetz—crowded the North Baltimore church to bid farewell to the 43-year-old Lutherville volunteer firefighter from Middle River who died Wednesday January 19th from injuries sustained while fighting a four-alarm apartment fire in Hillendale.

Mark Gray Falkenhan was born Dec. 26, 1967, in Middle River. Shortly after he graduated from Mount Carmel High School in 1986, Falkenhan joined the Middle River Volunteer Ambulance & Rescue Co. He rose to the rank of chief and became a lifetime member. 

Falkenhan then joined the Baltimore County Fire Department as an emergency medical technician in 1990.

He married Gladys on Nov. 11, 1993, and became an EMT-Paramedic the following year. He was an instructor at the Fire Rescue Academy and served at various stations across the county—Woodlawn, Dundalk, Golden Ring, Essex, Eastview and Fullerton—before retiring in 2006 to accept a job with the U.S.  Secret Service.  

“He loved his family first, but his life was the fire department,” his wife stated. Fire Chief Hohman could barely hold back the tears last week at Falkenhan’s house as he reflected on Falkenhan’s life and his devotion to public service. He first met Falkenhan more than two decades ago, when Hohman was the union president and he spent time speaking with those fresh out of the fire academy.

“He was so dedicated to what he did, and I could tell he loved what he did,” Hohman said. “You won’t be able to find a picture or photo out there of Mark that didn’t show that broad smile that went across his face. He enjoyed everything about his life.”

In addition to his affiliation with Lutherville VFC, Firefighter Falkenhan,  was a member of Baltimore County’s career fire department for 16 years, from 1990 to 2006. He was a paramedic/firefighter whose assignments included the Fire-Rescue Academy, where he was an instructor. He served at many stations, including Woodlawn, Dundalk, Golden Ring, Essex, Eastview and Fullerton. Falkenhan resigned in 2006 and was most recently employed with the U.S. Secret Service. In addition to his membership at Lutherville, he was a life member and past chief of the Middle River (MD)Volunteer Ambulance Rescue Co.

The Baltimore Sun newspaper published an editorial about the death of Firefighter Falkenhan that is required reading; HERE . An excerpt from the editorial reads as follows:

The word “hero” gets used too often to describe the most pedestrian of admirable behaviors, from the star quarterback who marches his team for a winning score to the kid who finds a missing wallet and turns it in. But exceptional bravery, special ability, exceptional deeds and noble qualities — those are what define an authentic hero, and Mr. Falkenhan lacked for none of them.

It was not by accidental circumstance or naiveté that he ended up on the third story of that Hillendale apartment complex in the midst of a fire, searching for missing residents. He knew the risks as well as anyone could. But his selfless desire to help others drove him forward into the flames.

That’s what made him exceptional. That’s why his legacy is important. That’s why the community is in his debt.

 

Think about this man; a brother firefighter, a husband,  a father, a mentor….reflect on his life, his sacrifice and the true meaning and definition of being a firefighter….

Reflect on what you do, who you are and what defines you; rise to meet the demands and challenges with the right qualities that have meaning and reflect upon the virtues of this noble profession we call the Fire Service.

 

Remembering Brackenridge 1991 Floor Collapse and LODD

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Remembering Brackenridge, Pennsylvania December 20, 1991: Four Firefighters Killed, Trapped by Floor Collapse

Four volunteer firefighters died when they were trapped by a partial floor collapse during a structure fire in Brackenridge, Pennsylvania, on the morning of December 20, 1991. All four were members of a mutual aid truck company that had responded to the early morning incident and were assigned to prevent fire extension from the basement to the ground floor of a 2-story building.

Although they were wearing full protective clothing and using self-contained breathing apparatus, it appears that they were overwhelmed by the severe fire conditions that erupted when a section of the ground floor collapsed into the basement.

The collapse cut off their primary escape path, and the fire burned through their hose line, leaving them without protection from the flames.  

  • For more on the incident and links to a series of incident reports, link here to Commandsafety.com
  • Current issues related to recent trends in floor collapse incidents, HERE

Vacant Residential Building Fires Report

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The Federal Emergency Management Agency’s (FEMA) United States Fire Administration (USFA) issued a special report examining the characteristics of fires in vacant residential buildings. The report, Vacant Residential Building Fires, was developed by USFA’s National Fire Data Center and is further evidence of FEMA’s commitment to sharing information with fire departments and first responders around the country to help them keep their communities safe.

The report is part of the Topical Fire Report Series and is based on 2006 to 2008 data from the National Fire Incident Reporting System (NFIRS). According to the report, an estimated 28,000 vacant residential building fires occur annually in the United States, resulting in an estimated average of 45 deaths, 225 injuries, and $900 million in property loss. Vacant residential fires are considered part of the residential fire problem as they comprise approximately 7 percent of residential building fires. In addition, intentional is the leading cause of vacant residential building fires which are more prevalent in July (9 percent), due in part to an increase in intentional fires on July 4 and 5. Finally, almost all vacant residential building fires are non-confined and half spread to involve the entire building.

The topical reports are designed to explore facets of the U.S. fire problem as depicted through data collected in NFIRS. Each topical report briefly addresses the nature of the specific fire or fire-related topic, highlights important findings from the data, and may suggest other resources to consider for further information. Also included are recent examples of fire incidents that demonstrate some of the issues addressed in the report or that put the report topic in context.

The report, Vacant Residential Building Fires,HERE

Findings

■ An estimated 28,000 vacant residential building fires are reported to U.S. fire departments each year and cause an estimated 45 deaths, 225 injuries, and $900 million in property loss.

■ Vacant residential building fires are considered part of the residential fire problem and comprise approximately 7 percent of all residential building fires.

■ Almost all vacant residential building fires are non-confined fires (over 99 percent).

■ Intentional is the leading cause of vacant residential building fires (37 percent).

■ Half of vacant residential building fires spread to involve the entire building. An additional 11 percent extend beyond the building to adjacent properties.

■ Bedrooms are the primary origin of all vacant residential building fires (12 percent). Following closely are common rooms such as dens, family and living rooms (10 percent), and cooking areas, kitchens (9 percent).

■ Vacant residential building fires are more prevalent in July (9 percent), due in part to an increase in intentional fires on July 4 and 5.

■ January 1, July 4 and 5, and October 31 have the highest incidence of vacant residential fires.

From 2006 to 2008, an estimated 28,000 vacant residential building fires were reported annually in the United States. The number of vacant residential buildings has always been seen as an issue in our society. These buildings are rarely maintained and often serve as a common site for illicit or illegal activity. In addition, vacant residential buildings are sometimes used by homeless people as temporary shelters or housing. A major concern when a vacant building catches fire is that little is known about the building’s overall condition.

Many buildings are in disrepair and can be missing certain structures, such as staircases or portions of floors. If individuals are known to use the vacant building as a residence, the unknown condition of the building and the unknown number of people using the building as shelter can put the firefighters’ lives in danger when they enter the building to attempt a rescue during a fire. The surrounding non-vacant properties are also at risk when vacant residential buildings catch fire.

It typically takes longer for vacant residential building fires to be detected as there are no occupants to be alerted by the smell or sound of the fires or respond to an alarm and the property loss is greater. In addition, if the fire has been intentionally set, especially with multiple ignition points, the damage can be greater, placing the lives of more individuals’ firefighters, adjacent residents, and any squatters in danger.

Fires in vacant residential buildings have become an even greater issue in the past few years. Many communities have seen an increase in the number of vacant residential buildings as the economy has declined; and with that an increase in the number of vacant residential building fires. From 2006 to 2008, intentionally set fires was the main cause of all vacant residential building fires (37 percent, as discussed later in this report), posing a serious issue for the community.

These types of fires continue to be a problem and concern within our society. “Devil’s Night” in Detroit, MI, is an example of the intentional fire issue in vacant properties. Prior to the late 1970s, October 30 or “Devil’s Night,” as it has been referred to in Detroit, was full of childhood pranks and minor vandalism acts. It was not until the late 1970s that this night of mischief went from being innocent to terrifying when arson became the leading cause of fire on Devil’s Night. Devil’s Night activity peaked in 1984 when over 800 fires were set in Detroit alone.

This issue of arson was exacerbated as Detroit was seeing a decrease in real estate values, resulting in some owners of vacant residences using the fires as a means to collect insurance dollars. This situation exists currently in Detroit (as well as other cities). In the 1990s, Detroit’s mayor took a major step in fighting Devil’s Night arson by renaming it “Angel’s Night” and calling upon police, firefighters, and local citizens to help patrol vacant properties that night and by cleaning up, or in some cases, removing the property entirely.

The efforts have proved effective but there is concern that the increase of vacant property within the past few years may lead to an upswing in fires in vacant and abandoned buildings. This topical report addresses the characteristics of vacant residential building fires reported to the National Fire Incident Reporting System (NFIRS) from 2006 to 2008. Vacant residential building fires, as analyzed in this report, include properties where the building is under construction, under major renovation, vacant and secured, vacant and unsecured, and being demolished. The remaining building status categories (occupied and operating; idle, not routinely used; building status, other; and undetermined) are considered “non-vacant” but not necessarily occupied. For the purpose of this report, the terms “residential fires” and “vacant residential fires” are synonymous with “residential building fires” and “vacant residential building fires,” 

From 2006 to 2008, an estimated 28,000 vacant residential building fires were reported annually in the United States. The number of vacant residential buildings has always been seen as an issue in our society. These buildings are rarely maintained and often serve as a common site for illicit or illegal activity. In addition, vacant residential buildings are sometimes used by homeless people as temporary shelters or housing. A major concern when a vacant building catches fire is that little is known about the building’s overall condition.

Many buildings are in disrepair and can be missing certain structures, such as staircases or portions of floors. If individuals are known to use the vacant building as a residence, the unknown condition of the building and the unknown number of people using the building as shelter can put the firefighters’ lives in danger when they enter the building to attempt a rescue during a fire. The surrounding non-vacant properties are also at risk when vacant residential buildings catch fire.

It typically takes longer for vacant residential building fires to be detected as there are no occupants to be alerted by the smell or sound of the fires or respond to an alarm and the property loss is greater. In addition, if the fire has been intentionally set, especially with multiple ignition points, the damage can be greater, placing the lives of more individuals’ firefighters, adjacent residents, and any squatters in danger.

Fires in vacant residential buildings have become an even greater issue in the past few years. Many communities have seen an increase in the number of vacant residential buildings as the economy has declined; and with that an increase in the number of vacant residential building fires. From 2006 to 2008, intentionally set fires was the main cause of all vacant residential building fires (37 percent, as discussed later in this report), posing a serious issue for the community.

These types of fires continue to be a problem and concern within our society. “Devil’s Night” in Detroit, MI, is an example of the intentional fire issue in vacant properties. Prior to the late 1970s, October 30 or “Devil’s Night,” as it has been referred to in Detroit, was full of childhood pranks and minor vandalism acts. It was not until the late 1970s that this night of mischief went from being innocent to terrifying when arson became the leading cause of fire on Devil’s Night. Devil’s Night activity peaked in 1984 when over 800 fires were set in Detroit alone.

This issue of arson was exacerbated as Detroit was seeing a decrease in real estate values, resulting in some owners of vacant residences using the fires as a means to collect insurance dollars. This situation exists currently in Detroit (as well as other cities). In the 1990s, Detroit’s mayor took a major step in fighting Devil’s Night arson by renaming it “Angel’s Night” and calling upon police, firefighters, and local citizens to help patrol vacant properties that night and by cleaning up, or in some cases, removing the property entirely.

The efforts have proved effective but there is concern that the increase of vacant property within the past few years may lead to an upswing in fires in vacant and abandoned buildings. This topical report addresses the characteristics of vacant residential building fires reported to the National Fire Incident Reporting System (NFIRS) from 2006 to 2008. Vacant residential building fires, as analyzed in this report, include properties where the building is under construction, under major renovation, vacant and secured, vacant and unsecured, and being demolished. The remaining building status categories (occupied and operating; idle, not routinely used; building status, other; and undetermined) are considered “non-vacant” but not necessarily occupied. For the purpose of this report, the terms “residential fires” and “vacant residential fires” are synonymous with “residential building fires” and “vacant residential building fires,” respectively. “Vacant residential fires” is used through-out the body of this report; the findings, tables, charts, headings, and footnotes reflect the full category, “vacant residential building fires.”

Additional References;

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