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Auto Parts Store Roof Collapse Double LODD 1996

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Roof Collapse Chesapeake VA 1996 Double LODD

OVERVIEW

On March 18, 1996, two firefighters were killed in Chesapeake, Virginia when they became trapped by a rapidly spreading fire in an auto parts store and a pre-engineered wood truss roof assembly collapsed on them. The cause of the fire was an electrical short created when a power company truck working in the rear of the building drove away with its boom in an elevated position, accidentally pulling an electrical feed line from the main breaker panel at the rear of the store.

Post-incident investigations indicate that the electrical fault may have sparked multiple points of fire origin throughout the roof structure of the building, due to improperly grounded wiring. At the time of the report issuance, this was exemplified as another incident illustrating the rapid failure of lightweight construction systems when key support components are involved in a fire. The report pointed out the importance of prefire planning and accurate size up by fire companies to determine the risk factors associated with a fire in this type of construction.

Lessons regarding importance of initial company actions, constant re-evaluation of action plans, strong command and coordination of units on the fireground, and recognition of signs of impending structural failure were also reinforced.

Reading through any number of NIOSH, USFA or NFPA reports, similar issues, challenges and operational factors resonate and continue to shape and challenge today’s fire ground operations.

It is without exception that the knowledge and insights being gained by the continuing efforts from the UL and NIST Research Studies coupled with the recommendations, from the NIOSH Fire Fighter Fatality Investigation and Prevention Program (HERE) will provide increased awareness and understanding of buildings, fire dynamics and the effectives of fire within the compartment, building and the manner in which fire departments engage in fire suppression operations.

Today’s fire ground is changing at a very rapid pace as it relates to the continued evolution, transition of engineered structural components and systems (ESS).

Are you prepared, knowledgeable and understand that new strategic and tactical approaches are required?

One of the most significant actions initiated by the Chesapeake Fire Department was the implementation of a Truss Identification Program (TIP).

Take a look at a past posting on CommandSafety.com where we published on an overview a few years ago of truss and engineering component systems across the United States HERE.

City of Chesapeake (VA) Truss ID Program, HERE

The following are excerpts and narrative from the USFA Technical Report Series TR-087 and NIOSH Report 96-17

Aerail Overview on Complex today

 

SUMMARY OF KEY ISSUES

Staffing : The first alarm response provided a small attack force with limited capabilities. The full response brought only 10 personnel.

Size-up : The first arriving company officer was not able to determine the location and extent of the hidden fire.

Pre-fire plan information: This complex required a pre-fire plan due to the complex arrangement, multiple occupancies, mixed construction, lack of fixed protection, limited access and difficult water supply problems. The first-due company did carry a pre-fire plan that showed the layout of the shopping center and the floor plan for the auto parts store, but the prefire plan was not referenced by the crew during the fire.

Delayed response: The first arriving company was on the scene alone for several minutes with only 3 personnel. The back-up companies had long response times. The lack of evidence of a working fire prompted the initial incident commander to return some of the responding units, resulting in even longer response times.

Water supply: The first-in company did not establish a water supply. This required the second engine company to be committed to this task.

Incident command: The battalion chief was faced with a complicated and rapidly changing situation. He was not able to effectively transfer command from the initial officer and direct the operations of widely separated units.

Operational risk management:The officers involved in the initial part of the operation had to make critical risk management decisions with limited information.

Accountability: Accountability for the personnel operating in the hazardous area was not established prior to the structural collapse. As the situation became critical, no one realized that a crew was still inside the building.

Rapid intervention crew: Additional crews did not arrive in time to assist the crew that was in trouble inside the building.

Radio communications: The lack of a clear radio channel for fire ground communications caused serious problems with command and control of the incident, including the failure to maintain communications with the crew inside and the failure to hear their request for assistance.

Lightweight construction: The roof collapsed quickly and with very little warning. This should be anticipated with a lightweight wood truss roof assembly. This hazard was not recognized by the crews on the scene.

BUILDING DESCRIPTIONConstruction and History

The fire occurred in a modern, lightweight construction building that was added to an existing strip mall in 1984. The older mall on exposure side four was separated from the fire building by a masonry fire wall and was constructed with masonry walls and a steel bar-joist roof structure. The exposures on side two consisted of additional stores that were similar in construction to the auto parts store. There were no exposures on sides one and three.

The auto parts store was constructed with two masonry exterior walls and two wood frame exterior walls, with a lightweight wood truss roof assembly. It was approximately 120 feet deep and 50 feet wide, providing about 6,000 square feet of open display and storage space. The roof assembly was a pre-engineered lightweight wood truss assembled from 2 x 6 top and bottom chords, with 2 x 4 web members held together with metal gusset plates.

  • There were no interior bearing walls or supports for the roof structure. At one end, the trusses were supported by a wood plate that was bolted to a metal beam.
  • The other end rested on top of the concrete block wall. Each truss was separated by 24 inches and they were covered with 1/2 inch CDX plywood sheathing under a two-ply rubber membrane.
  • A drywall ceiling was attached to the underside of the trusses, creating a truss void space (truss loft) 24 to 36 inches above the ceiling.
  • A sheet rock divider was located in the middle of the truss void as a draft stop. The roof had a slight pitch.
  • Three air handling units were on the roof of the building, with an estimated combined weight of 3,000 pounds. It is not known when these units were installed and they may have represented an unanticipated dead load on the roof assembly.
  • There was no indication that the trusses had been reinforced to support the extra weight of these units.
  • The original truss roof structure collapsed during the construction of the building, injuring three workers.
  • Most of the trusses were damaged and had to be replaced at the time. The fire building was occupied by Advance Auto Parts, a chain distributor of automobile part and lubricants. The store was designed with an open retail area containing display racks for goods.
  • A long counter ran from front to back behind which was shelving for additional auto parts. Waste oil and batteries were kept in a rear storage area separated from the front of the store by a drywall wall.
  • The southwest corner of the building contained employee restrooms which had a small water heater located in the ceiling space just above them. The main entrance to the store was through two large glass doors at the front of the building. A delivery and service entrance was located in the rear and a 40 foot trailer was parked behind the building and used for additional storage.

THE FIRE

At approximately 11:00 a.m. on March 18, 1996, a power company employee set up a service truck at the rear of the Indian River Shopping Center in Chesapeake, Virginia. The worker was going to disconnect the electrical power to a customer who had not paid an electrical bill. The customer, a cocktail lounge and bar, was located adjacent to Advance Auto Parts. In preparing to disconnect service, the power company worker elevated the articulating boom on his truck to roof level. Faced with the immediate loss of power, an employee of the lounge paid the electrical bill while the power company employee was beginning work, and went to the back of the store to show the receipt.

A stamped receipt indicates the bill was paid at 11:16 a.m. at a supermarket also located in the shopping center. The power company employee, working from the bucket of the articulating boom, lowered the boom and verified the receipt. Although the bucket had been lowered, the hinged elbow of the articulating boom remained elevated. The employee then radioed his supervisor from the cab of his truck, and received instructions not to disconnect power.

The power company employee then attempted to drive the service truck away, forgetting to secure the boom, which snagged on a power line feeding the meter at the rear of the Advance Auto Parts Store. This caused a phase-to-phase and phase-to-ground arcing fault at the store’s electrical meter, starting the fire. The power company employee immediately stopped, exited his truck, and cut the remaining power connections to the meter at the rear of Advance Auto Parts.

Initial Actions Prior to Calling 911

After cutting the power line to the building, the power company employee removed the meter, noticed smoke coming from the meter base, notified his office and requested that another power company crew and a supervisor come and assist him.

  • An employee of the Advance Auto Parts Store came to the rear of the building and met the power company employee, telling him that the store had lost electrical power and that a fire was being extinguished inside the building.
  • Another Advance Auto Parts employee discharged a dry chemical fire extinguisher on the spot fire that had started near the hot water heater above the employee restrooms.
  • All believed the fire had been extinguished at this time.
  • At 11:29 a.m., the Chesapeake Fire and Police Emergency Operations Center received a 911 call from Advance Auto Parts reporting a problem with the fuse box in the store.
  • The Chesapeake Fire Department was dispatched to a report of a fuse box sparking at 4345 Indian River Road at the Advance Auto Parts store.

Emergency Response

  • Initial response consisted of two engines, a ladder company, and a battalion chief, for a total of 10 personnel.
  • Engine 3 was the first due arriving company, responding from quarters. Engine 1 and Ladder 2 also responded.
  • Battalion 1 was dispatched as the command officer, but requested that Battalion 2 cover the assignment, since he was out of position.
  • Battalion 2 acknowledged the request, and he responded with the first alarm companies.
  • Engine 3’s crew consisted of three personnel: a driver/pump operator; Firefighter- Specialist John Hudgins, serving as Acting Lieutenant for the shift; and Firefighter- Specialist Frank Young, detailed to the station for the day, was riding in the jump seat. Engine 3 was responding in a reserve engine that had a 500 gallon water tank.

 

Initial Size-Up and Company Actions

At approximately 11:35 a.m., about five and a half minutes after dispatch, Engine 3 arrived on the scene at the front of the strip mall.

  • Hudgins reported “a single-story commercial structure, nothing showing from the front. Engine 3 is in command.”
  • Engine 3 took a position in front of the Advance Auto Parts Store. Hudgins and Young entered the structure from the front of the building to investigate.
  • Conditions were clear in the store, and there was no visible smoke or flames showing. They discovered light smoke near the electrical panel in the rear of the building, and radioed to Battalion 2 that they had a fire and were checking for extension.
  • Acting Lieutenant Hudgins then radioed for Engine 3’s driver to reposition the apparatus to the rear of the building.
  • Hudgins then radioed to Battalion 2, who had not yet arrived on the scene, that Engine 3 and Ladder 2 could handle the incident. Battalion 2 and Engine 1, the second due engine company, both went in service.

Engine 3 Reports They Are Trapped, Roof Collapses

At approximately 11:49 a.m., almost 20 minutes after the initial dispatch time, Hudgins radioed that he and Young could not get out of the building. Battalion 2 radioed back that he could not understand their transmission. Hudgins then radioed that they needed someone to come to the front of the building and get them out. Again unable to understand their transmission, Battalion 2 radioed for any unit on the fireground to advise him if they heard the message that was transmitted.

  • Engine 4 responded that they were unable to copy the transmission.
  • Engine 14 then marked on the scene and was instructed by Battalion 2 to lay a supply line to the front of the building. Battalion 1, enroute to the fire on the second alarm, radioed to Battalion 2 that it sounded like someone was trapped inside.
  • Battalion 3, also enroute, radioed that he would be on the scene momentarily and would assist.

At this time, Ladder 2’s crew was setting the outriggers and preparing to elevate their aerial ladder for defensive operations.

  • In the short time it took to accomplish the stabilization of the ladder truck, the front of the store became fully involved, the building contents ignited, and the roof collapsed.
  • Due to the radiant heat, Ladder 2 was forced to retract their outriggers and reposition to a safer defensive position on side one of the structure, and set up the aerial again.
  • Ladder 2’s crew did not hear Engine 3’s transmission that they were trapped.
  • Simultaneously, Engine 1 ran out of supply line about 200 feet short of the hydrant. Engine 2, responding on the second alarm, picked up the hydrant that Engine 1 was attempting to reach and laid a supply line to side one.
  • The driver of Engine 1 attempted to contact his officer by radio to advise that he could not reach the hydrant, but could not get through due to heavy radio traffic.
  • He parked the engine in the roadway, donned his SCBA, and went to the rear of the building to report to his Captain and rejoin his crew.
  • Battalion 3 arrived on side one about this time and radioed for all companies to switch to channel two, an alternate fireground tactical frequency.

Driven by the northerly wind and the draft created by the burning contents of the structure, the fire at the rear had grown in such intensity that personnel were forced to move Engine 3. Assisted by employees of the power company, Engine 3 was moved back away from the rear of the building. At 11:55 a.m., about 26 minutes after dispatch, the Captain of Engine 1, with his crew at the rear of the building, confirmed to Battalion 2 that “I got men on the inside from Engine 3, and the lines have been burned. I do not know their status, and we still have no water to go in after them.”

Battalion 3 met with Battalion 2 and discussed that they may have lost a crew inside. Battalion 3 assumed command and Battalion 2 went to the rear of the building to coordinate rescue efforts. There, Battalion 2 met with the Captain from Engine 1.

By this time, the building was fully involved and no rescue efforts could be mounted until the fire was knocked down. Officers at the front and the rear attempted to conduct a personnel accountability report (PAR) to determine who was missing and where they might be located.

  • An engine company responding on mutual aid from the Virginia Beach Fire Department was flagged down, connected to Engine 1’s supply line, and completed the water supply to a hydrant behind the shopping center within the City of Virginia Beach. Engine 3 was forced to move back once again, and the supply line was disconnected from Engine 3 and used to supply water to Engine 4, a telesquirt that was positioned for defensive operations at the rear.

Extinguishment and Body Recovery

The fire spread to the attic of the exposures on side two and was held in check by the fire wall on side four of the building. The fire was brought under control as the contents of the auto parts store burned off and several aerial streams were put into operation. After the fire was extinguished, a search for the missing firefighters was initiated. After the bodies of the firefighters were located, they were removed from the fire building by members of the Virginia Beach Fire Department, and transferred by members of the Chesapeake Fire Department to medic units.

The body recovery was supervised by the Chesapeake Fire Department Fire Marshal’s Office and documented. An investigation was immediately started by the Chesapeake Fire Department Fire Marshal.

ANALYSIS

Fire Cause and Flame Spread

  • The fire was caused by the electrical short created when the power company truck struck the power line to the building. Investigation by the City of Chesapeake Electrical Inspector after the fire revealed that the meter contained wiring that appeared to have been tampered with and did not comply with the electrical code.
  • Several connections at the meter had been double-lugged, connecting multiple wires to single terminals. Additional investigation by Virginia Power revealed that the building may have been improperly grounded, leading to numerous hot connections when the short circuit occurred. The main fuse did not trip at the breaker panel and the wiring on all three air handling units had been fused. This probably resulted in the ignition of multiple spot fires in the truss loft above the store.
  • It appears that the fires in the truss loft were still relatively minor when Engine 3 arrived, but the fire spread rapidly throughout the space due to the light wood construction.
  • The wind drawn from the open doors at the front of the building also promoted rapid fire growth. This would have created a tremendous hidden fire in the wood truss loft area despite clear conditions inside the structure.
  • Reports of heavy smoke and fire conditions on the roof at the same time Engine 3’s crew was calling for pike poles and personnel to come inside are indications towards this scenario.
  • The interior of the auto parts store contained racks of auto parts and supplies, including oil, lubricants, rubber, and plastic parts. The contents were packed closely together and stored in tall racks near the ceiling.
  • Once the fire had broken through the ceiling in the rear of the building, these contents would have quickly reached their ignition temperatures, creating flashover conditions in the rear of the store as the fire progressed, trapping the firefighters and forcing them to seek an exit at the front of the store.

Roof Collapse

  • The collapse of the pre-engineered truss roof occurred approximately 21 minutes after the time of dispatch, and within 35 minutes of the initial accident, that caused the electrical short.
  • The structure appears to have collapsed within 10 to 12 minutes after the truss space became heavily involved.
  • The collapse of similar truss assemblies under fire conditions within this time period has been well documented.
  • Post-incident investigations indicate that this truss assembly may have been weakened by deficiencies in the connection of the trusses to the beam on the east side of the building.
  • Also, the dead load of the three air conditioning units may have contributed to the rapid failure of the roof.
  • Reports from firefighters on the scene indicate that a partial failure of the truss assembly may have occurred in the rear of the building, followed shortly by the failure of the entire roof assembly.
  • It is possible that the crew of Engine 3 was trapped by the partial collapse of the roof in the rear, or by the collapse of racks containing auto parts in the building, or by the rapid spread of the fire and smoke which had broken through the ceiling.
  • It is also possible that a combination of these events occurred simultaneously. The failure of the entire roof assembly and complete involvement of the interior of the building with fire took place within one minute after the firefighters radioed for help, before any reaction to assist them could take place.

Fire Operations

 

Initial Response - The first alarm assignment was overwhelmed by the situation, the circumstances, and the unusual sequence of events that occurred at this incident. It is evident that a larger force would have been needed to initiate an effective offensive or defensive operation for a working fire in a 6,000 square foot commercial occupancy, with attached exposures on two sides, with or without the unusual complications.

  • The response of two engine companies, one ladder company and a battalion chief, provided a total of 25 only 10 personnel on the initial assignment.
  • The individual companies, which responded with three person crews, had limited capabilities to perform tasks independently.
  • This incident generated only a single call to 9-1-1 reporting an electrical problem.

 

LESSONS LEARNED AND REINFORCED

1. RISK ASSESSMENT is the primary responsibility of the incident commander.

This incident presented a very high risk to the firefighters who were attempting to make an interior attack. However, the risk factors were not recognized and the interior crew was not directed to abandon the building. Risk assessment should be a continual process, particularly when a situation is changing very quickly.

2. ACCOUNTABILITY is an essential function of the Incident Command System.

The location and operation of the initial attack crew was not tracked according to the incident command system that was in effect at the time of the fire. The system must keep track of the location, function, status, and assignment of every individual unit or company operating at the scene of an emergency incident. In order to be effective, the accountability process must be routinely initiated at the beginning of every incident and updated as the incident progresses and units are reassigned to different tasks.

3. TACTICAL RADIO CHANNELS are essential for firefighter safety.

The fireground operations were conducted on the same radio channel as the routine dispatch and transfer of additional units, hampering the fireground communications during the important early stages of the incident. Designated radio channels should be set aside specifically for communications between the incident commander and the units operating at the scene of an incident. The exchange of information, orders, instructions, warnings, and progress reports is essential to support safe and effective operations. Tactical channels should be assigned early and routinely to avoid the confusion that occurs when units that are already working are directed to switch to a different radio channel.

4. FIRE OPERATIONS must be limited to those functions that can be performed safely with the number of personnel that are available at the scene of an incident.

The initial response to this incident did not provide enough resources to safely initiate an effective interior attack for the situation that was encountered. The first arriving company initiated interior operations that could not be adequately performed or supported with the limited number of personnel at the scene or responding. The delayed arrival of back-up companies increased the risk exposure of the first due company. The situation called for a more conservative initial attack plan and/or an early retreat when the magnitude of the fire became evident.

5. WATER SUPPLY is a critical component of a safe and successful operation.

The failed attempt to establish an adequate and reliable water supply for the interior attack was a critical problem at this incident. This task occupied the second due engine company which was needed to provide either a back-up hose line to support the interior attack or a rapid intervention crew.

6. LIGHTWEIGHT WOOD TRUSS CONSTRUCTION is prone to rapid failure under fire conditions.

If the construction of the building had been known or recognized, the early failure of the roof structure should have been anticipated and the interior crew should have been withdrawn. This requires pre-fire planning to identify high risk properties and a reliable system to label the building or to inform the responding units of the risk factors of the building. It is usually difficult or impossible to make this determination when the building is burning.

Aerial View of the Current Auto Parts Store 2010

 

USFA Technical Report Series Incident Report: Tr-087 NFPA 1996 Report Summary Sheet: NFPAChesapeake

Near-Miss, with RIT Deployment at Structural Collapse: Canada

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A rapid and fast moving early morning fire in downtown Trenton, Ontario Canada resulted in the subsequent collapse of a three story mixed use commerical and apartment occupancy structure. Published media reports indicated the building was over 130 years of age and was in operation as an adult entertainment establishment on the lower level with multiple occupancy use apartments on the upper floors. The fire displaced 12 residents. The commercial portion of  the building on the number one floor was not operating at the time of the alarm.

For a complete overview of the general fire, refer to the links below for the media links.

Two firefighters were nearly trapped while engaged in primary search and rescue operations as the fire conditions deteriorated and compromise and collapse  conditions began to collapse the wood frame structure.

Pre-incident images clearly depict the typical building profile of a heritage type structure of the late 1880′s vintage with it’s sloping roof profile and window treatments that are evident on both the bravo and delta divisions (many with window mounted air conditioning units that constitute a collapse risk to operating companies on the ground perimeter) . As with many buildings in urban areas, the exterior envelope has been renovated in a manner that added an exterior metal clad panel system that is typically mechanically fastened directly to the facade or to a sub-assembly fastening system. This in effect covers the buildings originating facade, building materials and structural and cosmetic conditions.

Common to original building construction and layouts, the alpha division shows the manner in which the first floor wall has been modified with no indication of window locations and conditions in the upper floors. Common to this renovation technique is the placement of the metal facade directly over existing window openings and framing systems, resulting in either boarded and elimination of the window or the fames and glass still present within the interior room compartments compounding search and rescue assignments.

Sherwood Forest Inn, Image from Google Street View

 The metal exterior cladding masks the ability for arriving companies to identify if the structure is wood frame Type V, ordinary Type III or Brace Frame construction.  The profile and charactoristics of this building profile suggests a buidling of Type III Ordinary construction ( Brick and jost) with load bearing masony construction. This is not the case in this structure as fireground photos further depicted. The various fireground photos suggest that this was a wood frame structure with wood exterior sheathing with some brick masonry features applied to the alpha division. The building envelope is encased in a sheet metal panel cladding system attached the perimeter facade.

 

Delta Division, Google Street View Image

  

Image above shows the degree of interior fire involvement and smoke density. The sheet metal cladding that was applied to the surface facade masks the ability to monitor wall degradation and compromise, retains heat within the building envelope and has independent collapse considerations based upon the manner it is atached to the outer facade further compounding the structural integrity of the buildings wall envelope. Photo by Step Crosier.

In incidents taht have building profiles such as this, conservative risk management, establishment of primary and secondary collapse perimeters along the various divisions is imperative for firefighter safety and apparatus operabilty.

Collapse and failure of the primary structural support systems affecting both interior and exterior structural and infill systems. Photo by Marc Venema

The image above shows the extent of collapse. Look at the various construction features consisting of the original wood plank sheathing, brick facade work, wood framing system and the retrofitted metal paneling facade.  

  • How would you Read the Building based upon the pre incident photos shown at the being of this post?
  • Would you assume the building was a type III or IV structure or a wood frame or brace frame structure?
  • Does each building system have a different bearing on fireground operations, strategies, tactics and operational integrity and company and personnal safety?
  • How much operatoinal time do you have for a primary search and rescue assignment or for deployment and effective location of a fire seat and application of hose streams before you developing compromising conditions with the interior compartments?

 

Look at the brick veneer added to the wood sheathing covered by the metal panels in this image. Photo by Steph Crosier

 

 

 

   

 

Fire Dynamics Simulation of 2011 Baltimore County LODD- 30 Dowling Circle

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Operations at 30 Dowling Circle 01.19.2011 Box 11-09

 On Wednesday, January 19, 2011, a fire occurred in an apartment building located in the Hillendale section of Baltimore County, Maryland. This fire resulted in the line of duty death (LODD) of volunteer firefighter Mark G. Falkenhan, who was operating as the acting lieutenant on Squad 303 . Upon their arrival, FF Falkenhan and a second firefighter from Squad 303 deployed to the upper floors of the apartment building to conduct search and rescue operations. Other fire department units were already involved with both firefighting operations and effecting rescues of trapped civilians.

During these operations, FF Falkenhan and his partner became trapped in a third floor apartment by rapidly spreading fire and smoke conditions. The second firefighter was able to self-egress the building by diving headfirst down a ladder on the front (address side) of the building. FF Falkenhan declared a “MAYDAY” and implemented “MAYDAY” procedures, but was unable to escape or be rescued.

FF Falkenhan was located and removed via a balcony on the third floor in the rear of the building. Resuscitative efforts began immediately upon removal from the balcony, and continued en route to the hospital. FF Falkenhan succumbed to his injuries and was pronounced deceased at the hospital.

Mark Gray Falkenhan had dedicated his life to serving others. He perished in the line of duty on January 19, 2011 while performing search and rescue operations at a multi-alarm apartment fire in Hillendale, Baltimore County (Maryland). He was 43 years old.

 

Firefighter Mark Falkenhan

30 Dowling Circle

 

The Baltimore County (MD) Fire Department published the Line of Duty Death Investgation Report of the 30 Dowling Circle Fire recently.

The report was written by a Line of Duty Death Investigation Team comprised of departmental members, including representatives of the local firefighters’ union and the Baltimore County Volunteer Firemen’s Association.

An overview and executive narrative of the final report (PDF) on the apartment fire where Volunteer Firefighter Mark Falkenhan sustained fatal injuries was posed on CommandSafety.com HERE.

FF Mark Falkenhan

 On Wednesday, January 19, 2011, a fire occurred in an apartment building located in the Hillendale section of Baltimore County, Maryland. This fire resulted in the line of duty death (LODD) of volunteer firefighter Mark G. Falkenhan, who was operating as the acting lieutenant on Squad 303 (for purposes of this report, Mark will be referred to as FF Falkenhan).

Upon their arrival, FF Falkenhan and a second firefighter (FF # 2) from Squad 303 deployed to the upper floors of the apartment building to conduct search and rescue operations. Other fire department units were already involved with both firefighting operations and effecting rescues of trapped civilians.

During these operations, FF Falkenhan and FF # 2 became trapped in a third floor apartment by rapidly spreading fire and smoke conditions. FF # 2 was able to self-egress the building by diving headfirst down a ladder on the front (address side) of the building. FF Falkenhan declared a “MAYDAY” and implemented “MAYDAY” procedures, but was unable to escape or be rescued.

FF Falkenhan was located and removed via a balcony on the third floor in the rear of the building. Resuscitative efforts began immediately upon removal from the balcony, and continued en route to the hospital. FF Falkenhan succumbed to his injuries and was pronounced deceased at the hospital.

The investigating team examined any and all data available, including independent analysis of the self contained breathing apparatus (SCBA), turnout gear and autopsy report. The Bureau of Alcohol, Tobacco, Firearms and Explosives (ATF) produced a fire model to assist with evaluating fire behavior. Multiple site inspections were conducted. Extensive interviews were conducted by the team which also attended those conducted by investigators from the National Institute for Occupational Safety and Health (NIOSH). Photographic and audio transcripts were also thoroughly analyzed. A comprehensive timeline of events was developed. All information used to make decisions regarding recommendations was corroborated by at least two sources.

  • In fairness to those units involved in this incident, the investigating team had the advantage of examining this incident over the period of several months. Furthermore, given the size and nature of the event, and the fact that arriving crews were met with serious fire conditions and several residents trapped and in immediate danger, all personnel should be commended for their efforts for performing several rescues which prevented an even greater tragedy.
  • The team did not identify a particular primary reason for FF Falkenhan’s death.
  • What were identified were many secondary issues involving but not limited to crew integrity, incident command, strategy and tactics, and communications.
  • These issues are identified and discussed, and recommendations are made in appropriate sections of the report, as well as in a consolidated format in the Report Appendix.

Some of the issues identified in this report may require some type of change to current practices, policies, procedures or equipment. Most, however, do not. Specifically, the analysis and recommendations regarding Incident Command and Strategy and Tactics show that if current policies and procedures are adhered to, the opportunity for catastrophic problems may be reduced.

  • Mark Falkenhan was a well-respected and experienced firefighter.
  • He died performing his duties during a very complex incident with severe fire conditions and unique fire behavior coupled with the immediate need to perform multiple rescues of victims in imminent danger.
  • It would be easy if one particular failure of the system could be identified as the cause of this tragedy.
  • We could fix it and move on. Unfortunately it is not that simple.
  • No incident is “routine”. Mark’s death and this report reinforce that fact.

On Wednesday, January 19, 2011 at 1816 hours, a call was received at the Baltimore County 911 Center from a female occupant at 30 Dowling Circle in the Hillendale section of Baltimore County. The caller stated that her stove was on fire and the fire was spreading to the surrounding cabinets. Fire box 11-09 was dispatched by Baltimore County Fire Dispatch (Dispatch) at 1818 hours consisting of four engine companies, two truck companies, a floodlight unit, and a battalion chief. All units responded on Talkgroup 1-2.

The location, approximately one mile from the first dispatched engine company, is a three story garden-type apartment complex, with brick construction and a composite shingle, truss supported roof. The fire building contained a total of six apartments divided by a common enclosed stairway in the center with one apartment on the left and one to the right of the stairs.

 

Fire Dynamics Simulation of 2011 Baltimore County LODD- 30 Dowling

Fire Dynamics Analysis and Insights

 

INTRODUCTION:

Assistance from the Bureau of Alcohol, Tobacco, Firearms and Explosives (ATF) Fire Research Laboratory (FRL) was requested for a fire at 30 Dowling Circle by the Baltimore County Fire Investigation Division (FID) through the ATF Baltimore Field Division on the night of January 19, 2011.

ATF Fire Protection Engineers were asked to utilize engineering analysis methods, including computer fire modeling, to assist with determining the route of fire spread and the events that led to the firefighter MAYDAY and subsequent Line of Duty Death.

Download the REPORT HERE

BACKGROUND:

Working closely with the Post Incident Analysis Team, the ATF Fire Research Laboratory created a computer simulation of the garden apartment building using Fire Dynamics Simulator (FDS). FDS is a computational fluid dynamics (CFD) modeling program developed by the National Institute of Standards and Technology (NIST).

FDS utilizes mathematical calculations to predict the flow of heat, smoke and other products of fire. Smokeview, a post-processer computer program also produced by NIST, was then used to visualize the mathematical output from FDS. The most current available versions of both programs were used: FDS 5.5.3 and Smokeview 5.6. Below are photographs of the front and rear of the fire building next to an image of the same building constructed in FDS.

Figure 01. 30 Dowling Street

 

Figure 2. FDS representation of the front of 30 Dowling Circle showing the terrace (T), second (A) and third (B) levels.

 

The garden apartment building at 30 Dowling Circle was attached to two similar garden apartment buildings, one on each side. The fire damage was isolated to 30 Dowling Circle, so the exposure buildings were not included in the computer fire model. The entire six unit garden apartment building was modeled in FDS, including the patio and balconies on the rear of the building. FDS works by dividing a space into cubical “grid cells” for calculation purposes. FDS then computes various CFD calculations for each grid cell to predict the movement of mass, energy, momentum and species throughout a three-dimensional space.

The Dowling Circle model consisted of 2,560,000 total grid cells that were each 3.9 inch (10 cm) cubes. The model was used to simulate a total elapsed real time of 27.5 minutes, beginning before the 911 call and ending just after flashover of the third floor and the firefighter MAYDAY.

The model was synchronized in real time with the fireground audio throughout the duration of the fire.

Fiqure 03 and 04

 

FDS has been validated to predict the movement of heat and smoke throughout a compartment, however the accuracy of fire modeling depends on it being used appropriately by a trained user that is aware of its limitations. Due to lack of knowledge about the exact material properties for the various furnishings and other available fuels, a user-specified fire progression was used for this application.

For flame and fire gas movement after consumption of the original burning fuel packages, the fire model calculated smoke and ventilation flow paths through the building and was used to gain a better understanding of the rapid fire growth leading to flashover of the stairwell and third floor.

  • In addition, FDS was utilized to illustrate the complex route of fire spread through the building as verified by witness statements, firefighter interviews, photographs and burn patterns.
  • Input data for the computer model included heat release rate data and video from previous testing conducted by the ATF FRL and NIST.
  • Ambient weather data was also input into the model, including temperature, as well as wind direction and magnitude at the time of the fire. In addition, several alternative compartmentation scenarios were modeled to explore the possible effects of closed stairway apartment entrance doors on the spread of smoke and flames in the stairwell.
  • The statements of each firefighter were reviewed and their individual actions (breaking windows, opening doors, etc.) and observations (fire size, smoke conditions, etc.) were recorded on floor diagrams.

The actions and observations of the firefighters were then associated with specific times in the fireground audio to generate an overall event timeline. All events in the model are based on this master timeline of events. In addition, all photographs were time stamped and synchronized with the model. The Post Incident Analysis Team was consulted throughout the development of the event timeline and the computer fire model to ensure accuracy.

MODELING ANALYSIS:

1. Analysis of Fire Development in the Terrace Level

The fire originated on the stovetop of an occupied apartment on the right (south) side of the terrace level (apartment T2). Flames from a grease fire ignited kitchen cabinets, eventually causing the kitchen to flashover into the attached living room. Upon fire department arrival, a fully developed fire existed in the living room and kitchen of apartment T2. Prior to exiting the apartment, the occupant opened both the rear sliding door and the apartment entrance door in an attempt to ventilate smoke from the apartment.

 

Figure 06. A typical floor plan of the right side apartments at 30 Dowling Circle.

 

An analysis of the ventilation flow path through the apartment with FDS indicated that a significant unidirectional flow path existed up the stairs with an inlet at the rear terrace sliding door and outlet at the front apartment entrance door leading to the stairwell.

Figure 7. Smokeview frame of the rear of the building indicating the fire origin and smoke spread within the T2 apartment. Figure 8. View of smoke flow out of kitchen and open sliding glass door (center of photo) in the rear of apartment T2. Figure 9. Smokeview frame of flashover of the kitchen with flames extending into the living room. Flames also begin to extend out of the rear sliding door and impact the balcony above.

 

Figure 10. Ignition of second level balcony resulting from flame extension from living room.

 

This unidirectional flow path up the stairs is difficult to combat and is often experienced during basement fires as crews attempt to descend interior stairs. The model indicates sustained air temperatures in the stairwell of approximately 600 Fahrenheit (315 Celsius) at velocities of approximately 6 mph (2.7 m/s) from floor to ceiling as crews attempted to descend the stairs. This is consistent with statements from firefighting crews, who experienced extremely high heat conditions and indicated periodically seeing flames in the smoke layer flowing up the stairs.

The elevated air velocity of the stairwell flow path resulted in a high rate of convective energy transfer to the structural firefighting gear and high perceived temperatures as the firefighters attempted to descend the stairs. Firefighting crews flowed a hoseline down the stairs to combat the high temperatures; however no significant cooling was noticed by firefighters because the hose stream could not reach the seat of the fully developed fire in the kitchen area.

The crews were simply cooling the ventilation flow path without cooling the source of the energy in the apartment. It was not until a hose stream was directed through an exterior window and a portion of the fire was extinguished that gas temperatures and velocities began to decrease, allowing firefighters to make entry to the terrace apartment via the stairs.

Figure 12. Smokeview section frame showing unidirectional flow of approximately 600 Fahrenheit (315 Celsius) gases out of the stairwell entrance door

Front photo of unidirectional flow of smoke up stairwell from apartment T2. Note the high volume of smoke from floor to ceiling as the stairwell door serves as the flow path outlet. The ground ladder in the foreground was used to rescue an occupant on the third floor trapped by heavy smoke in the stairwell. (Refer to Figure 014)

Figure 014. Front photo of unidirectional flow of smoke up stairwell from apartment T2. Note the high volume of smoke from floor to ceiling as the stairwell door serves as the flow path outlet.

 

The first arriving engine, E-11, was staffed with a Captain, Lieutenant, Driver/Operator, and a Firefighter. Upon arrival at 1820 hours, the Captain gave a brief initial report describing a three story garden apartment with smoke showing from side Alpha: “The Captain of E-11 will have Command and we are initiating an aggressive interior attack with a 1 ¾” hand line”. Command also instructed the second due engine to bring him a supply line from the hydrant. 

A female resident (victim # 1) appeared in a third floor apartment window, Alpha/Bravo side (Apt. B-1), yelled for assistance, and threatened to jump. Smoke or fire was visible from any of the third floor windows. At 1823 hours, Command advised Dispatch that he had a rescue and that he was establishing Limited Command. Fire Dispatch was in the process of upgrading the response profile to an apartment fire with rescue when the responding Battalion Chief requested that the fire box be upgraded to a fire rescue box. While the Firefighter and Lieutenant prepared for entry into the building, the Captain and Driver/Operator extended a ladder to the 3rd floor apartment window and rescued the resident. The first attempt by the Firefighter and Lieutenant to make entry into the side Alpha entrance was unsuccessful due to the extreme heat and smoke conditions.

The second due engine, E-10, arrived at 1823 with staffing of a Captain, Lieutenant, Driver/Operator, and a Firefighter. At 1823, E-10’s crew brought a 4″ supply line to E-11 from the hydrant at Deanwood Rd. and Dowling Circle and assisted the first-in crew with fire attack.

  • The Captain from E-10 conferred with Command and was instructed to advance a second 1 ¾” hand line.
  • The window to the first floor right apartment (Apt. T-2) was removed, and the second 1 ¾” line was advanced to the building by the crew of E-10.
  • Fire attack was initiated through the removed window. At 1827, Command requested a second alarm.

At this time, heat and smoke conditions just inside the front door improved enough to allow the Firefighter and Lieutenant from E-11 to make entry through the front door and into the stairwell. There they encountered heavy, thick black smoke and high heat conditions coming up the stairs from the terrace level apartment. The Lieutenant reported that the doorway to the first floor apartment was orange with fire and he had to fight his way through heavy heat and smoke conditions to attack the fire in the first floor right apartment (Apt. T-2). Entry was made approximately 3 feet into the doorway when the Firefighter’s low air alarm began to sound, and he exited the building. A member from E-10’s crew replaced the Firefighter from E-11 on the hose line.

At the same time, the Captain from E-11 proceeded to the rear of the structure to complete his initial 360 degree size up. He noted that there was fire emanating from the open sliding doors on the first floor Charlie/Delta apartment (Apt. T-2), extending to the balcony above. E-1, staffed by a Captain, Driver/Operator, and two Firefighters arrived and completed the hookup of the supply line that had been laid to the hydrant by E-10. The rest of Engine 1’s crew grabbed tools and an extension ladder and reported to the Charlie side of the building.

Figure 015 Charlie Side ( Rear) Extension

The Photo above referenced as  Figure 015 shows conditions  from rear of flames in apartment T2 and extension to the balcony above. Note the relative minimal volume of smoke as the sliding door serves as the inlet for ventilation into the apartment. The smoke and heat is flowing in from the rear, through the apartment and up the stairs.

This unidirectional flow path up the stairs is difficult to combat and is often experienced during basement fires as crews attempt to descend interior stairs.

  • The model indicates sustained air temperatures in the stairwell of approximately 600 Fahrenheit (315 Celsius) at velocities of approximately 6 mph (2.7 m/s) from floor to ceiling as crews attempted to descend the stairs.
  • This is consistent with statements from firefighting crews, who experienced extremely high heat conditions and indicated periodically seeing flames in the smoke layer flowing up the stairs.
  • The elevated air velocity of the stairwell flow path resulted in a high rate of convective energy transfer to the structural firefighting gear and high perceived temperatures as the firefighters attempted to descend the stairs.

Firefighting crews flowed a hoseline down the stairs to combat the high temperatures; however no significant cooling was noticed by firefighters because the hose stream could not reach the seat of the fully developed fire in the kitchen area.

The crews were simply cooling the ventilation flow path without cooling the source of the energy in the apartment.

It was not until a hose stream was directed through an exterior window and a portion of the fire was extinguished that gas temperatures and velocities began to decrease, allowing firefighters to make entry to the terrace apartment via the stairs.

Plan view of flow path and temperatures within the apartment. Note the location of the seat of the fire and the location of initial hose stream application down the stairs.

Figure 016

 

Photograph of hoselines being positioned at the stairwell entrance door and front window. Note the heavy smoke venting from all front openings in apartment T2. (Figure 017)

Figure 017 Alpha Side Entry Door

 

Figure 017  Hoselines being positioned at the stairwell entrance door and front window. Rapid Fire Progression Leading to Flashover of the Third LevelFlames extended upwards from the T2 apartment sliding door and ignited the rear balconies of the second and third level apartments above.
 
Fire on the second floor balcony extended into apartment A2 by failing the sliding glass door and igniting vertical plastic slat curtains that were suspended above.As crews searched within the second floor apartment, they noted seeing the burning curtains on the floor with flames extending to a nearby couch (containing polyurethane foam padding) adjacent to the sliding doorway.
 
The fire continued to grow unsuppressed and spread to a second couch as interior firefighting crews were engaged in rescuing two victims from the living room in the second floor apartment.Personnel stated that at this point fire conditions seemed to improve, suggesting that crews were making progress extinguishing the fire. (The first arriving attack crew reported that they were able to see apparatus lights through the sliding doors on Charlie side, which indicated to them that smoke and fire conditions were improving.)Truck 1, a tiller unit staffed by a Lieutenant, two Driver/Operators, and a Firefighter, arrived on side Alpha and immediately began search and rescue operations.
 
Windows on the second floor Alpha/Delta side apartment (Apt. A-2) were vented and ladders were thrown to gain access. T-8 arrived at the alley on side Charlie. E-1 extended a ground ladder to the third floor balcony on the Charlie/Bravo side of the structure (Apt. B-1), and made access to the apartment to search for additional victims.They noted fire venting from the first floor Charlie/Delta apartment (Apt. T-2) out of the sliding glass doors progressing upwards towards the balcony on the second floor.
 
Upon entering the apartment, they conducted a primary search and noted minimal heat with light smoke conditions.The crew accessed the hallway via the apartment entry door and noticed an increase in the temperature and the amount of smoke.They immediately closed the door and exited the apartment via the ground ladder.Upon exiting the apartment, E-1’s crew observed E-292 on the scene with a hand line extending into the apartment of origin, (first floor, Charlie/Delta side, Apt. T-2).
 
The officer on E-1 noted white smoke coming from the unit.Having already laid a supply line from the intersection of the alley and Deanwood Road, E-292’s crew extended a 1 ¾” hand line into the apartment of origin. Moderate fire conditions with zero visibility were encountered, and they reported feeling a great deal of heat on their knees as they crawled through the apartment.The Lieutenant and the Firefighter from Truck-1 entered Apartment A-2 via a second floor bedroom window (Alpha/Delta side) and began a search for additional victims. As they traversed the living room area they found an unconscious male resident (victim #2).
 
At 1836 hours, the Lieutenant notified Command via an urgent transmission that a victim had been located and they needed assistance with evacuation. The Lieutenant and Firefighter noted a small fire in the rear corner near the victim as they exited the room. The crew returned to the bedroom from which they had entered and closed the door behind them. Victim #2 was then evacuated from the apartment via a ground ladder through the bedroom window, and transferred to EMS personnel on side Alpha.
 
Figure 019 Flame extension and suppression efforts at the rear of the structure. Flames caused the second level glass slider to fail and ignite plastic curtains in the doorway located
 

Figure 019

 
 

The middle level apartment (A2) entrance door was opened by a second search crew around the same time as the second couch ignited, creating a ventilation flow path from the second floor balcony, through the apartment, and upwards into the stairwell (third floor). This flow path follows the same general route through the apartment and into the stairwell as was seen in the terrace level apartment below. Squad 303’s crew arrived on scene after the bulk of the fire in the terrace level apartment had been suppressed and appeared to be under control. The crew entered the front stairwell, which had minimal smoke up to the second level and the crew began to systematically search the building.

Squad 303’s crew proceeded to search two apartments before entering the third floor right side apartment to conduct a search, leaving the entrance door open. It should also be noted that carpeting impacted the bottom of the door and prevented the apartment entrance doors on the second and third levels from closing automatically. The entry doors had to be actively pushed closed to overcome the friction of the carpet.

 

Photo depicting building smoke and fire conditions around the arrival of Squad 303.

Note the lack of heavy smoke or fire in the stairwell or terrace level.

There is also no indication of the growing fire in the second (middle) level apartment.

 

 

 

When Squad 303’s crew of two firefighters entered the third level apartment (B2), smoke was banked about halfway down the walls with moderate visibility. The crew could clearly see the floor of the apartment without the need to crawl below the smoke layer to search. Squad 303’s crew was unaware of the flames spreading across the two couches in the second floor apartment below them. The crew split in order to search the apartment faster, with one firefighter searching the front bedrooms and the officer searching the kitchen and living room.

As flames in the second level began to rollover into the apartment entranceway, the smoke layer in the third level quickly dropped to the floor with a rapid increase in temperature. With Squad 303’s crew searching above, flames began to extend into the stairwell, supplied by sufficient ventilation flowing through the apartment. This combination of fuel, heat and oxygen rich fresh air resulted in a rapid increase in heat release rate and flashover of the second level apartment followed by full room involvement.

The open entrance doors on the second and third levels created a ventilation flow path through the second floor apartment, into the sealed stairwell and up through the third floor apartment directly above. The flames followed this flow path and extended from the second floor, through the stairwell and into the living room area of the third floor apartment. Flashover of the third floor occurred approximately 30 seconds after the second floor experienced flashover.

Figure 026 and 027

 

Rollover from the second level apartment into the stairwell.

 

 
 
Flames followed the ventilation flow path and extend into the third floor apartment, resulting in ignition of the couches just inside the doorway.

 

 

    

 

Command sounded the building evacuation tones as flames extended into the hallway and up to the third level apartment.

Two couches just inside the entrance door on the third level ignited, blocking the primary means of egress for both firefighters from Squad 303. Upon hearing the evacuation horns from the trucks, the second firefighter from Squad 303 (searching the front bedrooms) attempted to exit the apartment via the apartment entrance door, however he was blocked by flames in the living room and stairwell.

Trapped in the bedroom, the firefighter bailed out headfirst down a ground ladder on the front side from the third floor. Squad 303 officer’s means of egress through the apartment entrance door was also blocked by the flames in the living room and stairwell. There were no windows located in the rear of the apartment.

The only means of escape was the balcony slider, however the entire balcony was engulfed in flames from the fully involved apartment below. With both escape routes blocked by flames and experiencing extremely high heat conditions, Squad 303’s officer requested assistance and declared a MAYDAY from the rear of the third floor apartment.

Firefighters re-entered the structure to combat the fire and locate the trapped firefighter. The downed firefighter was eventually located on the third level just inside the sliding glass door and was removed to the rear balcony. The firefighter was then extricated in a stokes rescue basket down the aerial ladder of a truck located in the rear, where he was subsequently transported to the hospital.

Effects of Compartmentation on Fire Spread

The Post Incident Analysis Team requested that alternate modeling scenarios be conducted to explore the effects of compartmentation on fire spread throughout the building.

The team specifically wanted to know how the ventilation flow paths through the stairwell would differ if the second or third level apartment entry doors were shut after entering/leaving the apartments. Two alternate computer fire modeling scenarios were conducted.

The first alternative modeling run featured the exact same fire scenario, except the second (middle) level apartment door was closed after the last victim was removed from that apartment. The apartment entry doors from the stairwell were fire-rated doors constructed of solid wood.

  • As soon as the door is shut, the ventilation flow path through the apartment and up the stairwell is blocked.

 

Shutting the second level apartment door blocks the flow path and flame extension into the stairwell. 

Even with the third floor apartment door left open, the model indicates that the stairwell and third floor remain tenable for firefighters. Flames eventually extend from the third floor balcony into the apartment, however the escape routes through the stairwell and the front apartment windows are accessible.           

The model indicates that closing the second level apartment door prevents the flow of smoke, heat and other products of combustion from entering the stairwell, thus preventing flashover of the stairwell and the third level. As long as the second floor entry door remains shut, the model indicated that the conditions within the stairwell and third floor remain tenable for firefighters, even with the third floor apartment door open.

A second alternative modeling scenario was conducted where the third level entrance door was closed after crews made entry to search the apartment.The same fire conditions from the actual model were used.When the door remained closed, the outlet of the ventilation flow path was blocked at the top of the stairs. Without a complete flow path, there wasn’t sufficient oxygen flowing through the second floor apartment to support extended burning in the stairwell.

Consequently after flashover of the second floor, the flames in the stairwell only exist momentarily before consuming all available oxygen and becoming ventilation limited.The fire model indicated that temperatures within the third floor apartment stayed tenable for firefighters, even with a fully developed fire on the second floor and flames in the stairwell.

Flames would eventually extend up the rear balcony to the third level, however they would not block egress through the living room and front windows of the apartment.By closing the apartment door on the third floor and blocking the outlet for fire gases emanating from the second floor apartment, the third floor apartment remains tenable for firefighting crews and the temperatures only briefly spike in the stairwell before the fire becomes ventilation limited.The ventilation flow through the apartments results in an increased burning rate within both the second and third levels, as well as the stairwell.                     

Results of each modeling scenario describing extent of flame spread

Results of each modeling scenario describing extent of flame spread.

 
 
 
 
 
 
 
 
 
 
The Effects of Compartmentation on Fire Damage to the StructureThe impact of compartmentation on fire and smoke spread is evident by examining the post-fire damage throughout the structure. While other factors contributed to the relative fire damage, including fire department overhaul and relative apartment configuration, analyzing the damage to the building and the position of the apartment entry doors provides insight on the benefits of compartmentation.

By closing apartment unit entrance doors and interior hollow core doors, one can slow or even block the ventilation flow path through the structure, thus significantly reducing the rate of fire spread. The photos below represent the post-fire damage in all six apartments within the fire building. Four of the six apartment entry doors were open for the majority of the fire and the relative difference in damage is clearly evident.

Terrace level stairwell landing looking into T1 (left) and T2 (right) apartments.

 

Door Closed……Door Open

 

 

Using doors to compartmentalize and limit fire and smoke spread in a structure is not limited to fire-rated entrance doors. Interior hollow core doors also offer considerable protection for compartmentation purposes.

A search crew utilizing the Vent, Enter and Search (VES) technique through a front window used a hollow core bedroom door to isolate themselves from the developing fire in the living room of apartment A2.

As the crews removed the second victim from the living room to the bedroom, they shut the bedroom hollow core door behind them.

The living room soon experienced flashover followed by full room involvement, however the bedroom remained isolated from the heat and smoke for the duration of the fire. The photos below illustrate this effective use of compartmentation to protect firefighters during a search.

 
Controling the Doors during VES

 

 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
 
SUMMARY:
While no fire model will exactly replicate a fire, this model provided insight on the route of fire spread, the rapid fire growth leading to flashover of the second and third level, and the benefits of compartmentation on slowing fire and smoke spread.
  • The unidirectional flow path up the stairs from the terrace level apartment resulted in a high rate of convective heat transfer to the firefighters initially attempting to descend the stairs, making attacking the seat of the fire very difficult.
  • The model then supported the fact that the main stairwell acted as an open channel for fire and smoke spread between the second and third levels, resulting in flashover of the third level in approximately 30 seconds after the second level.
  • This rapid fire growth leading to flashover is supported by photographs, witness statements and fireground audio.
  • The model was then utilized to explore the effects of compartmentation using apartment entrance doors.
  • The FDS model supported the scene observations and indicated that shutting the entrance doors blocked the flow of buoyancy driven fire gases through the structure, ultimately preventing fire extension to the third floor apartment via the stairwell.
  • The FDS model was utilized as part of the overall engineering analysis of this tragic fire and allowed for a better understanding of the events that led to the firefighter MAYDAY and subsequent Line of Duty Death.
  • The model was also used as an educational tool providing insight on potential methods of preventing similar tragedies in the future.
  • The results of this engineering analysis are intended to be reviewed by the Post Incident Analysis Team to assist in the creation of recommendations to mitigate the danger associated with future fire incidents.

References:

FDNY All Hands Fire

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Box 661 Private Dwelling All Hands Fire

Sunday, January 23, 2011 9:06 hrs FDNY Rescue 2 responded to 628 Lafayette Ave. for a fire on the 2nd floor of a 3 story private dwelling.

Operational Conditions can Change in a Heartbeat: Remembering FDNY Black Sunday

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Take the time to read both NIOSH reports and remember the sacrafice…

Three veteran FDNY firefighters died in the LODD in Brooklyn, New York and the Bronx on Sunday January 23, 2005, a day that has become known as “Black Sunday” and called one of the saddest in fire department history. Two firefighters were killed and four others were badly hurt when they were forced to jump from a fourth-floor window of a burning building in the Bronx.

Later, a third firefighter died after tackling a basement blaze in Brooklyn.Lt. Curtis Meyran, 46, of Battalion 26, and Firefighter John Bellew, 37, of Ladder 27, died after battling the Bronx blaze on East 178th Street in the Morris Heights section.

Three firefighters were in critical condition at St. Barnabas, and a fourth was in serious condition at Jacobi Medical Center. Six Bronx firefighters became trapped in the building while searching for people on the fourth floor. When the fire from the third floor broke through to the fourth, they were faced with a horrifying choice. They jumped out a fourth-floor window, knowing that they would be critically injured.

Firefighters Jeffrey Cool, Joseph DiBernardo, Eugene Stolowski, and Cawley were badly hurt in the Bronx fire. They were trapped on the fourth floor and were left with the life-or-death choice of leaping 50 feet or burning up. The Brooklyn firefighter, Richard Sclafani, 37, died at a hospital after being injured at a two-alarm fire in the East New York section.

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